Emulsion Treatment Program
Emulsion Treatment Program
SPE 25346
Emulsion Treatment Program
Roslan M. Soffian and T.L. Niven, Esso Production Malaysia Inc.
Copyright 1993, Society of Petroleum Engineers, Inc.
This paper was prepared for presentation at the SPE Intemational Meeting on Petroleum Engineering held in Singapore, 8-10 February 1993.
This paper was selected for presentation by an SPE Program Committee following review of information contained in an abstract submitted by the author(s). The
material, as presented, does not necessarily reflect any position of the Society of Petroleum Engineers, its officers, or members. Papers presented at the SPE
meetings are subject to pUblication review by the Editorial Committees of the Society of Petroleum Engineers. Permission to copy is restricted to an abstract of not
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ABSTRACT
INTRODUCTION
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Chemical Trials
Following the pilot test, EPMI conducted further
chemical field trials at Guntong A to verify the
performance of the chemical in the system. Figure 8
illustrates the results when 20 ppm chemical was
injected into the Guntong A stream. With 20 %
BS&W leaving the production header, almost all of
the water was knocked-out in the first stage separator,
with less than 0.5% BS&W leaving the vessel.
When the cold satellite streams were commingled
with the warmer Guntong A crude, some freewater
knockout occured. With commingled temperature of
around 45-50oC in the surge vessel, the best effluent
that could be achieved was 2-3% BS&W, reflecting a
substantial removal of water.
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Trea1ment Solutions
Consideration was geven to the installation of
insulated pipelines from both the Guntong and Tabu
satellites to raise the temperature of the crude arriving
at Guntong A and aid in demulsification. However,
this solution was found to be not suitable in view of
the following:
o
2.
3.
4.
ACKNOWLEDGEMENT
The authors wish to thank the management of Esso
Production Malaysia Inc. and PETRONAS for
permission to publish this work.
SPE 25346
GUB
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EXISTrNO CENTRAl
EMISTINt) SATElliTE
FUTURE' CENTRAL
o FUTURE SI.. TELUTE
SPE25346
WATER
PRODUCTION 8
IKBWI'D)
..
.T
YEAR
TE~~ln.LO~D
SE'IES M BOTTLE
TESTS CONDUCTED
IlUNTOftQ. TAIllI
ANt1 'AlAt
.HYOQATtQN
INSTALLtD
S UOIES
tl \/SnoOK CllEMlCAL
WfJEcnON FACilITY
1Jt93 JN$tAllATtON
2) fNSUlAT!b PWlINES
lUSS33"" NOT REoUlRED
3) FUllICAt.. PROJECT
(USS21M) FOR l,ABU
NOT JUSftFlEO -lESS
COSTlVALThNATlYE
BEINo PURSUED
nVlAfF'VtlCTTL
C'''AM.''''
TEST FINOttfOS
2) CIlEM'CAl
Sf l D
HEeE REeOMMENDAnoNS:
IV CHEMICAL
T"ALS TO
~~c=TIOATE
PLATFOJt~
2) DHE....INE
PERFORMANCE
TREATMENT
NOTE:
REQ....EMENTS
(-). SHUT..'" OF HIGH WATERCUT WE'llS REDUCES TME ACTUAL TOTAL WATER
,RODUCTION IN COMfl'ARtSON TO TNt FoREeas T RATEs..
'00r-----------------------------,
_
PIIOCUS IlI!QUMtMElfTt
., TtMOPATUIll!IIlI!TPTION TIME/SPAllATION EffICIENCY
_
TUT_TOflEUlTlll4lU
TESTEQ"""" GP_
NEAT P_.--AIlATOIlIIIlYDIlOCYCl.ONE
C_ _ ''''US$UOIC
1'lL0T TEiT ICHE....TIC
'I
NOT 011.. NX
GUAWELLS
QUAlBte MUl
1L-_T_AB_U_ _
--'I---l><I~1 I
CHEMICAL
IN.JtCl"lOft
J
~_.
"
TEITSE'
__ ~_1
:---------- ........
---~
TESTSEP)
SPE 25346
TABU:
PERCENT
WATER
REMAlMHO
OU~
HEAT REQUJJII!D
NO CHEMICAlI
6D% BS&W POSSIBLE
'.0:0
'--..~ ..~I
10
TEMPRATUllE /'CI
0.1" 8.&.
.I.W
2-8
cn.l.w