Project On Cycle Time
Project On Cycle Time
A Project Report
On
(Asst. Professor)
Year 2016-17
CERTIFICATE
This is to certify that the project report entitled
Year 2016-17
A
PROJECT REPORT
ON
By
AND
It is intended a matter of pride for me to get selected for the project work
activity in such an esteemed organization.
I would like to express my deep sense of gratitude towards the Mr. Ashwini
Maheshwari Sir – President – BU (Forging), Mr. Sanjay Shinde Sir – Plant Head –
VEPL VII (Forging), our mentors from Varroc Engineering Pvt. Ltd. – VII (F), Mr.
Vijay Deshpande Sir – Asst. Manager - (Prod.), Mr. Narendra Bagde Sir –
Executive Engineer - (Prod.) and Late.Santosh Talikhedkar– Senior Officer – HRD
for giving me such attention and time.
At the same time, I express my sincere thanks towards all the persons from
Varroc Engineering Pvt. Ltd. – VII (F), for their guidance and encouragement.
I also thank Dr. R.S. Pawar – Principal, Prof. G. S. Dhage – Head of the
Department & Prof. Deepak Pawar – Guide. Shreeyash College of Engineering &
Technology, Aurangabad for their constant supervision.
i
ABSTARCT
This way we can say that all these KAIZENS will prove to be efficient in terms
of reducing the cycle time and thereby increasing the productivity also reducing the
cost till some extent.
ii
INDEX
iii
3.2.8 Ball formation on Up-setter 2 11
3.2.9 Slot milling on AMS 11
4 Project on Ball Turning Machine (CNC) 13
4.1 Study of Machine 13
4.2 Problem definition 14
4.3 Kaizen idea 14
4.3.1 Problem status 14
4.3.2 Kaizen 14
4.4 Program before kaizen 15
4.5 Tool History 18
4.6 Raw material 20
4.7 Program after kaizen 23
4.8 Reduction in cycle time 26
4.9 Comparative table of parameters before and after kaizen 26
4.10 Test to ensure that the quality of product is maintained 26
even after changing the specification
4.11 Benefits 27
4.11.1 Cost saving 27
4.11.2 Productivity increases 28
4.11.3 Time saving 29
4.12 Kaizen sheet 30
5 Results 31
6 Conclusion…...…………………………………………….. 32
References…………………………………………………. 33
Appendices 34
A In Plant Training Certificate 34
B Paper publish Certificate 35
C Article Review Card 36
iv
FIGURE INDEX
v
GRAPH INDEX
vi
TABLE INDEX
vii
Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
CHAPTER 01
INTRODUCTION
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
forging include hot, warm and cold forging, heat treatment, post heat treatment
machining and soft machining. The division has a dedicated modern crankshaft facility
to cater to the commercial vehicle segment. In addition, a strong program management
capability provides developmental support to its key customers. The manufacturing
capabilities of crankshaft include forging and testing, and the engineering capabilities
include design & drafting, simulation, post processor - tool path and product design.
For that of valves, the manufacturing capabilities include heat treatment, pattern
hardening, extrusion forging, hommel inspection, induction hardening and ultrasonic
inspection. Varroc also operates an international forging plant in Italy that supplies
large forgings to Caterpillar in Europe for construction equipment.
Present Investment :
Website : www.Varrocgroup.com
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
1) Sauer Danfoss
2) Royal Enfield
3) Eaton
4) Ognibene
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
The Forge business supplies forged and machined parts for engine and
also manufacturing 6 cylinder crankshafts for commercial vehicles and stationary
engines. Key products such as 2, 3 and 4 Wheeler engine parts, which include
transmission gears and assemblies, crank pins, connecting rods, flanges, Ring gears,
Crankshafts, Camshafts, Knuckles, Front Axle Beams and hydraulic components
which are supplied to leading OEMs as well as Tier 1 suppliers in India and is also
exported to Europe. The division has 3 manufacturing plants and an Engineering
center in India as well as 1 manufacturing plant in Italy, which caters to heavy
undercarriage parts.
1.8 Vision
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
1.9 Mission
1.10 Quality
TPM Policy
CHAPTER 02
LITERATURE REVIEW
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
CHAPTER 03
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
Raw Material
The process of annealing takes near about 16 hours for completion and the
temperature in the annealing furnace is maximum up to 690® C.
The setup consists of 4 tanks containing water, puls solution and dryer
too. Basket should be loaded with 100-150 pieces and should be immersed in water
keeping it there for 3 minutes approx. Basket should be dried then in dryer followed
by immersing it into puls solution. The load is then kept into it for around 5 minutes
and then dried. After unloading it is then send to Up setter I for cap formation on
hydraulic press
3.2.4 Upset –I
Pulse coated slug is pressed under load upto 70 T on the hydraulic press having
capacity of 150 T. This pressure causes the phenomenon of cap formation. The load
applied by the press is not fixed instead it keeps on varying depending upon the
hardness of the slug.
3.2.5 Pre-Machining
Turning is a machining process in which a cutting tool, typically a non-
rotary tool bit, describes a helical tool path by moving more or less linearly while the
work piece rotates. The tool's axes of movement may be literally a straight line, or
they may be along some set of curves or angles, but they are essentially linear (in the
nonmathematical sense). Usually the term "turning" is reserved for the generation of
external surfaces by this cutting action. Turning operation is carried out on cap formed
slug for pre-machining purpose.
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
milling. They can also be built into a “gang” to machine more than one surface in the
same plane at the same time.
b) End Milling
End milling is selected for shorter, shallower slots, especially closed grooves
and pockets, and for milling key-ways. End mills are the only tools that can mill
closed slots that are: Straight, curved or angled Wider than tool diameter, designated
pockets. Heavier slotting operations are often performed using long edge milling
cutters.
After all these processes the job is then sent to heat treatment shop and then
ultimately to Final Inspection Department and then dispatched.
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
CHAPTER 04
The ball turning operation is carried out on CNC machine, which is provided
by FANUC PVT LTD. In this operation two inserts are used one having 0.8 mm
radius and another having 0.4 mm radius which are used for rough & finish cut
purpose respectively.
4.3.2 Kaizen:-
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
00000 ;
N1 ;
G40 ;
T0101 ;
G50 S1800 ;
X-28.0 ;
Z1.6 ;
G0 Z2.5 X-28.0 ;
G0 Z1.0 ;
G0 Z2.0 X-28.0 ;
G0 Z0.5 ;
G0 Z1.5 X-20.0 ;
G01 Z0.4 ;
G01 Z-22.5 ;
G40 G0 X-30.0 ;
G0 Z1.0 ;
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
G0.X-20.0 ;
G01 Z0.3 ;
G1 G41 X-21.9 ;
G1 X-16.2 Z-15.35 ;
G1 Z-21.5 ;
M01 ;
N2 ;
G40 ;
T0202 ;
G50 S1800 ;
M04 ;
G96 S210 ;
G0 Z50.0 M8 ;
X25.0 ;
G0 Z0.0 ;
G1 X-3.0 F0.2 ;
G0 X18.5 Z1.0 ;
G1 X21.5 Z-0.5 ;
G1 X15.0 Z-15.402 ;
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
G1 Z-24.5 ;
G1 X14.4 Z-26.2 ;
Z-26.8 ;
M09 ;
M05 ;
M11 ;
M30 ;
For reduction in cycle time I changed parameter of CNC like speed, feed & number of
cuts from 3 to 2, but it was affecting on tool life. Production was increased but tool life
decreased at the same time cost of operation was also increased, which ultimately
increased the cost of product.
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100
80
60 Tool life in NOS
40
20
0
2400 2600 2800 3000
Speed in rpm
In CNC for operation earlier 0.8MM insert of Sandvik coromant was used for rough
operation, which was increasing the cost of operation and cost of product as well.
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
For ball turning operation in CNC 0.4 mm insert was used for finishing operation.
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
Selection of Insert
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
First of all, decide Positive whether positive or negative style inserts are going to
be used. A negative insert has an angle of 90° (0° clearance angle), while a positive
insert has an angle of less than 90° (7° clearance angle). The illustration of the
negative style insert shows how the insert is mounted in the holder and tilted.
1. Single sided
2. Low cutting forces
3. Side clearance
4. First choice for internal turning and for external turning of slender components
5. 7°Clearance angle
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
Changes in Program:-
For selected material I change parameter in program like feed, speed, and
number of cut or pass, for reducing cycle time of ball turning machine.
Changed program as follow:-
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
00000 ;
N1 ;
G40 ;
T0101 ;
G50 S1800 ;
X-28.0 ;
Z1.6 ;
G0 Z2.5 X-28.0 ;
G0 Z1.0 ;
G0 Z2.0 X-28.0 ;
G0 Z0.5 ;
G0 Z1.5 X-20.0 ;
G01 Z0.4 ;
G01 Z-22.5 ;
G40 G0 X-30.0 ;
G0 Z1.0 ;
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
G0.X-20.0 ;
G01 Z0.3 ;
G1 G41 X-21.9 ;
G1 X-16.2 Z-15.35 ;
G1 Z-21.5 ;
M01 ;
N2 ;
G40 ;
T0202 ;
G50 S1800 ;
M04 ;
G96 S210 ;
G0 Z50.0 M8 ;
X25.0 ;
G0 Z0.0 ;
G1 X-3.0 F0.2 ;
G0 X18.5 Z1.0 ;
G1 X21.5 Z-0.5 ;
G1 X15.0 Z-15.402 ;
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
G1 Z-24.5 ;
G1 X14.4 Z-26.2 ;
Z-26.8 ;
M09 ;
M05 ;
M11 ;
M30 ;
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
Due to change in parameters like speed and feed and reducing the number of
stroke or pass the cycle time gets reduced .Following table indicates how productivity
is increased after the Kaizen.
4.10 Test to ensure that the quality of product is maintained even after
changing the specification
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
4.11 Benefits
Before Kaizen
After kaizen
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
Before kaizen
After every 150 NOS we changed corner of insert and after using all insert
corners i.e. after 900 NOS an insert was changed.
Time required for changing an insert for each corner : 5 min ( for 150 NOS )
Time required for changing an insert for all 6 corners : 30 min ( for 900 NOS )
Time required for changing insert in one month =[ Total number of insert used
in one month ] X [Time required for changing insert for all 6 corner]
= 58 x 30 = 1740 min (for 51840 NOS )
Time required for changing insert in one year = 1740 x 12 = 20880 min ( for
622080 )
After kaizen
After every 400 NOS we change corner of insert and after 2400 NOS we
change an insert.
Time required for changing insert in one year for 622080 NOS = 21.6 x 30 x
12 = 7776 min
Total time saving due to changing insert in one year = Time required for
changing insert in one year before kaizen - Time required for changing insert
in one year after kaizen
= 20736 – 7776 = 12960 min=216 hrs = 9 day
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
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CHAPTER 05
RESULTS
= 211454 INR
6 Total time saving due to changing insert in one year: 12960 min=216 hrs
= 9 days
7 Total time saving due to changing insert in one year for 2 machine : 18 days
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Cost and Cycle Time Reduction of Ball Turning Operation of Cardan Shaft
CHAPTER 06
CONCLUSIONS
Productivity increases
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REFERENCE
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