Apollo Experience Report Command and Service Module Electrical Power Distribution Subsystem
Apollo Experience Report Command and Service Module Electrical Power Distribution Subsystem
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by Robert E . Mzlnford and Bob Hendrix
Lylzdoa B, Johnson Space Center
Houston, Texas 77058
19. Security Classif. (of this report) 20. Security Classif. (of this page) 21. NO. of Pages 22. Price
* For sale by the National Technical Information Service, Springfield, Virginia 22151
NASA- MSC
CONTENTS
Section Page
SUMMARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1
INTRODUCTION ................................... 2
Grounding. .................................... 7
Sensors . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8
Inverter.. .................................... 11
COMPONENTS. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
Motor Switches . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13
Circuit Breakers . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15
Relays . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16
iii
FIGURES
Figure Page
2 Battery circuits . . . . . . . . . . . . . . . . . . . . . . . . . . 5
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APOLLO EXPERIENCE REFORT
COMMAND AND SERV ICE MODULE
ELECTR ICAL FOWER D ISTR I BUT1ON SUBSYSTEM
B y Robert E. M u n f o r d and Bob Hendrix
Lyndon B. Johnson Space Center
SUMMARY
The Apollo command and service module electrical power distribution subsystem
was required to receive electrical power from any combination of seven direct-current
sources (three fuel cells, three entry batteries, and one service module battery) and
to condition, control, and deliver the power to the appropriate loads. To satisfy these
requirements, the system was designed to perform the following functions.
4. Protect the various power sources from a malfunction in the loads or the
wiring
5 . Protect each power source from a malfunction in any other power source
Major developmental effort w a s expended on the static inverter, the most complex
electrical unit in the system; therefore, the history and design configurations of this
device are discussed in detail in this report. Conversely, the motor-driven switch
(which, electrically, is a relatively simple device) proved to be quite troublesome
because of its complicated mechanical design and widespread u s e throughout the corn-
I mand and service module. It is discussed in this report, and special emphasis is
placed on problems that developed during the Apollo P r o g r a m . The developmental
efforts and problems with other allied equipment are also reviewed.
Although numerous minor changes were made as a result of real ,or anticipated
problems, the overall system performance was satisfactory throughout the program.
Nevertheless, several recommendations worthy of consideration in the design of any
new system a r e apparent f r o m a review of the entire effort. Most of the recommenda-
tions were made as a result of many incidents rather than a particular problem and
are not specifically addressed in the text of the report, but are discussed m o r e fully
in the recommendations and concluding remarks.
INTRODUCTION
Throughout the active life of each Apollo vehicle, beginning with the initial power-
up and continuing through checkout, flight, and postflight testing, the command and
service module (CSM) electrical power distribution subsystem (EPDS) was used almost
continually. Three fuel cells located in the service module (SM) provided the primary
source of power for the major portion of a mission. The fuel cell output was supple-
mented by two of the three 40-ampere-hour command module (CM) entry batteries
during high-load phases of the mission and was backed up by a 400-ampere-hour
battery in the SM (added after the flight of Apollo 13), which could be used if a fuel cell
failed. The electrical configurations of the spacecraft during various phases of a
normal mission are described in the following paragraphs.
Near the end of the launch countdown period, the fuel cells were activated and
remained active until CM/SM separation. A few minutes before lift-off, two entry
batteries were connected to the main buses to provide power to the CM in the event of
an abort. After the spacecraft was in orbit, the entry batteries were disconnected,
recharged, and used only to supplement fuel cell power during service propulsion
system (SPS) burns. Between burns, the load normally varied between 60 and
80 amperes (well within the capability of the fuel cells) ; however, when gimbals
were operated during SPS burns, the load could reach 120 amperes, requiring the
additional capacity of the two entry batteries.
All three entry batteries were switched to on-line status during preparation f o r
entry and became, a t CM/SM separation, the sole source of electrical power for the
vehicle. During descent, the load w a s approximately 60 a m p e r e s and continued near
that level until the vehicle w a s 800 feet above water and the main buses were deener-
gized. After this time, only the recovery aids and various small loads on the post-
landing bus required electrical power.
The EPDS of the Apollo CSM w a s designed to control, condition, and deliver I
nominal 28 V dc and 115 V ac power. These tasks had to be accomplished with maximum I
reliability, flexibility, and safety yet remain within weight and volume constraints. To
satisfy these goals, the system was designed around two main buses in the direct-
current system and two buses in the alternating-current system. j
The direct-current system (fig. 1) accepted power from three fuel cells and
three entry batteries and distributed this power to two main direct-current buses.
Loads on the buses were divided into the following three categories according t o
criticality and power source.
I
1. Nonredundant essential loads were fed from both buses through isolation diodes. I
2. Redundant essential loads were arranged so that loads were fed f r o m different
buses. I
2 I
A
n
Bat battery
OL overload
I y: OL and RC
, S,Mbs;A+:r?S,M,b:;
OL and RC
, SMbusArTv: SM bus B
OL and RC
R C reverse current
Fuel cell 1 Fuel cell 2 Auxiliary Fuel cell 3
3
either or both main buses. Although the pyrotechnics were not a p a r t of the EPDS,
provisions were made f o r using main entry battery power to fire the explosive devices
if the pyrotechnic batteries failed.
Together with the normal precautions taken in any electrical installation to pro-
tect the user from shock and t h e hardware from physical damage, the primary con-
c e r n s in the design of the EPDS were for mission safety and for the protection of the
power sources from downstream faults and fault propagation if problems did arise.
Diodes, circuit breakers, fuses, and r e v e r s e and overcurrent s e n s o r s were used to
protect power sources.
Because components of the EPDS were distributed throughout the CSM, the
system was exposed to a variety of environments including water, urine, salt, and
dust. Atmospheric p r e s s u r e varied from sea level t o the vacuum of deep space, and
temperatures varied widely. In addition, equipment in the CM p r e s s u r e vessel had
t o be capable of maintaining mechanical integrity when exposed to a 78g impact shock
if touchdown occurred on land. Verification that the equipment could withstand these
environments was determined by qualification testing.
All the precautions mentioned previously were considered during the design,
fabrication, and testing of the system to ensure crew safety and mission success. To
improve the performance of the system further, the EPDS design was continuously
reviewed, and each change or proposed change was evaluated in t e r m s of reliability.
The performance of the system during test and flight was reviewed t o determine if any
problems existed that might require design changes.
SYSTEM DESCRIPTION
Three fuel cells in the SM provided the bulk of the power f o r a normal mission.
Any fuel cell could be connected t o either or both of the main buses, but the normal
configurations were with fuel cells 1 and 2 on main bus A and with fuel cell 3 on main
bus B. After a cryogenic supply failure, which resulted in the loss of all t h r e e fuel
cells on Apollo 13, an auxiliary battery was added in the SM to supplement the
remaining power s o u r c e s if one or m o r e fuel cells failed.
A battery charger was provided to recharge the entry batteries from fuel cell
power. The charger used both alternating current and direct current to apply a
current-limited charge to one battery at a time. After being used, each battery was
recharged as soon as practical to provide maximum power for entry or any contingency.
As time passed, the need for added flexibility of power s o u r c e s became apparent,
resulting in the addition of circuit breaker (CB) 15 and CB24 (fig. 2) to make it possible
I postlanding
a:nd h-2 -0 4
9-
1
BOA
5
t o put any battery on any bus in the power system. In addition, CB18 and CB19 were
added to permit activation of a pyrotechnic bus by a n entry battery if a need occurred.
Although many other minor changes were made in both design and procedures, the
system and system components remained basically the s a m e as those flown in 1966 on
spacecraft 009, the f i r s t Block I vehicle launched f r o m the NASA John F. Kennedy
Space Center. The m o r e significant of these changes are reviewed in the following
discussion.
The large circuit breakers on the output of the entry batteries were directly
attached to the battery-mounting hardware to protect the wires leading t o the f i r s t
control panel. Overload and reverse-current s e n s o r s for each fuel cell (fig. 3) served
a similar purpose in the SM.
Main bus A
Fuel cell bus disconnect
L
power
I I
I 1 TO all fuel cell
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bus control u
state I
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I switch
I
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I TobusB
I I control
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6
A timing circuit (fig. 4) in the reac- Note
tion control system (RCS) provided automat- K13 - AUTO RCS transfer
relay lsystem A)
ic switching to connect the entry batteries K14 - AUTO RCS transfer Bat
to the main buses in the event of a pad relay (system 6)
(Activated by CSM
abort. This feature allowed battery power seoarationl
to be conserved by operating the vehicle
from ground power until just before lift- Bat charger,
off. Jf a n abort was necessary, crew ac- voltmeter, and
tion was not required to provide power to
the CM after separation from the SM. 0
Main bus tie OFF
bat AIC
AUTO
Groundi ng r-----------
I RCS
I
dc negative bus ac neutral bus Pyro negative bus Shield ground bus
1
A
CM load
T
Inverters
1
Pyro bat load
CM wire
CM load R shielding
T Pyro bat
SM load negative
?-l
dc negative bus
SM load
cell negative terminal
Jettison sequence control negative terminal
SM
*
Shield ground bus
SM wire
shielding
Sensors
Sensors monitored the main direct-current buses for low voltage (fig. 7) and
signaled the caution and warning (C&W) system if the voltage level fell below 26.25 volts.
Alternating-current buses were monitored by s e n s o r s (fig. 8) f o r low voltage, overload,
and overvoltage. If either the load o r voltage went out of limits, a C&W signal was
initiated; however, of the three anomalous conditions, only a n overvoltage condition
required corrective action to be taken faster than a crewmember could react to the
situation. Therefore, an overvoltage condition resulted in automatic disconnection of
the faulty inverter.
8
Main Comparator
(sensor)
- -
Amplifier Lamp
driver
~ Main busA
0 OFF
i i
19
Caution and warning lamp power
Regulator
r--
I
-
1 Main
busA
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Main
buss
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Control Units
The greatest concentration of control functions in any single unit was in the SM
power distribution box. This box, located on the upper deck of the SM, contained both
automatic and remotely actuated motor switches t o control direct current in the SM.
Fuel cell outputs could be connected t o either CM bus by motor switches that provided
r e v e r s e current and overload protection. Provisions also were included f o r switching
ground support equipment power to the vehicle and for protecting the buses if a heater
short occurred in the environmental control subsystem.
The CM direct-current power control box used motor-driven switches and stud-
mounted diodes to switch power output from the CM batteries to the main buses. To
achieve maximum heat transfer, the diodes were mounted directly on plated heat
sinks; the plating was the only electrical insulation between the diode mounting base
and the heat sink. Early in the test program, several failures occurred when the
insulation was damaged and the diode shorted to ground. This problem w a s overcome
by using plated washers between the diode a:id the heat sink; as a result, a t least two
failures in the plating were required before a short would occur.
The battery charger (fig. 9) also was modified after fabrication because the
output was originally calibrated for a particular current and wire routing. However,
subsequent reconfiguration of the wiring and the addition of circuit breakers resulted
in a buildup of tolerances which, when combined, caused the charger output t o be
inadequate. The unit had t o be partly depotted to gain a c c e s s to the potentiometer that
controlled the output voltage level. Setting the potentiometer control a t the proper
level solved the problem.
To K 1 j
* Transformer Current Auxiliary Battery C
AC 1 rectifier amplifier power
o r 2 +B
K? power
circuit supply
115 V supply
400 Hz
9 A f f
Figure 9. - Functional diagram of battery charger.
I nverter
During the initial phases of the Apollo Program (1962 and 1963), studies were
performed to determine the most feasible power system for motor applications.
Because of these studies, a central inverter system was selected instead of individual
inverters for each application. This system w a s chosen because it had the lowest
weight and greatest reliability. Inverters were designed with an output capability of
1250 volt-amperes, making it possible for a single unit to supply all the alternating
current required by the vehicle (fig. 10). Three such inverters were needed on each
vehicle to meet the reliability requirements for mission success and crew safety.
After the essential requirements were established, the inverter was designed to meet
the following criteria.
3. Frequency: 400 hertz with 6400 hertz external timing; 400 * 7 h e r t z when
f r e e running
11
B~ck-hst Harmonic
dc filter (three - L Filter
35 V Power inverter
(eight stages)
c neutralizing
amplifiers) transformer
SCR t Filter
--- Demodulator ac filter
h
1.6 kHz Zener
I
-
1.6 kHz and bridge
demodulated signal
signal Magnetic
amplifier 4
' Zener
diode
Current
-
-
4
A1
B1
-
1 reference c1
A sensing m A2
bridge
transformers 82
1.6 kHz c2
~
+2 - LOW
mltage
control 400 Hz
-
6.4 k&
-
Eight-stage
digital count-
down
Overcurrent
trip circuit
-
-
Figure 10. - Inverter block diagram.
The inverter housing was redesigned for Block II spacecraft inverters to facilitate
easy removal for repair purposes. At the s a m e time, output connectors were installed
in place of the terminals that were used on e a r l i e r models. Another change to the
inverter was made after the Apollo 204 fire. The inverter housing w a s sealed to pre-
vent propagation of f i r e if any component within the inverter ignited. This inverter
became the -0008 model.
The -0008 model was installed on the first s e r i e s of Block 11 spacecraft and
performed satisfactorily; however, the manufacturer of the power-switching transistors
used in the inverters experienced difficulties in meeting delivery schedules. Conse-
quently, a second s o u r c e w a s selected to supply transistors with s i m i l a r characteristics.
The transistors from the second source had a slightly faster switching speed than the
original ones; therefore, minor circuit modifications had to be incorporated, resulting
in the -0010 inverter configuration. The -0010 model was f i r s t flown on the Apollo 10
mission and performance was normal. Although the design w a s not altered after this
configuration, thermal-acceptance testing of all black boxes became mandatory l a t e r
in the Apollo Program. A s a result, the -0008 and -0010 units became, after testing,
the -0012 and -0014 units, respectively.
12
L
failure being caused by a fast timeout o r premature tripping of the inverter. This
condition was tolerable; therefore, no further changes were made.
COMPONENTS
From To fuel
ac bus
1 or 2
cell 3 Motor Switches
- C I -- pump
13
Although some motor-switch problems
occurred during flight, the majority of the
problems resulted from ground t e s t s and
operation. The motor switches proved to
b e extremely sensitive to mishandling,
improper operation, or incorrect control
circuitry. Most of the failures resulted
from the application of a low control voltage
or the simultaneous application of "on" and
"off" commands. Both misapplications
resulted in excessive buildup of heat and
subsequent destruction of the motor. These
problems were overcome, in part, by
using special test consoles to test any equip-
ment that contained motor switches and by
providing s t r i c t procedures f o r operating
the motor switches.
A m o r e s e r i o u s problem became
apparent after the Apollo 14 mission. As a
result of an investigation, a new failure mode
of the motor switch w a s discovered. A
switch in the direct-current power control
Figure 12.- Motor switch assembly. box failed in midtravel. When the switch
was opened for inspection, it was found that
the motor a r m a t u r e had undergone exces-
sive heating and the a r m a t u r e windings had opened. Additional investigation and
disassembly of the motor showed that the commutator b a r s were separated f r o m the
rotor and presented evidence of extreme heat in the a r e a of the brush/commutator
interface. Furthermore, the buildup of residue on the commutator was far g r e a t e r
than normal.
14
During a thorough investigation, many switches were tested and then disassembled
to facilitate a microscopic examination of the mechanism. No abnormal conditions were
found in the g e a r train or other mechanical parts of the switch, and, in all anomalies of
this type, it was determined that the motor was at fault. Small silicone grommets, used
as seals in the motor housing, were not cured under uniform conditions; those not cured
completely tended to r e v e r t to their precured condition. This reversion process was
present at all temperatures; however, heat aggravated the condition. A s the reversion
progressed, the catalyst that was used for curing the silicone w a s released and migrated
to the motor commutator where it combined with bearing oil and brush residue to f o r m
a high-resistance deposit between the brushes and commutator. This deposit resulted
in excessive heat being generated at the interface, a low a r m a t u r e current, and,
consequently, low motor torque. Loss of torque caused the motor to stall until the heat
generated within the motor was sufficient to cause a wire in the a r m a t u r e to open.
Motor-current t r a c e s , which depict the time required for the switch to transfer,
and the amplitude of the current were taken before each operable switch was disas-
sembled. These t r a c e s were compared with similar t r a c e s taken by the vendor during
the fabrication of the switches. As a result of numerous t r a c e evaluations, the t r a n s f e r
time, which proved to be a reliable indicator of the condition of a motor commutator,
was used to identify switches with potential motor problems. The evaluation also estab-
lished a maximum time in which a switch with a clean commutator should transfer; conse-
quently, current t r a c e s were made for all switches in several phases of the checkout to
determine the transfer time of each. Any switch with excessive transfer time was
replaced.
Ci rcui t B reaker s
Several difficulties were experienced during the qualification testing of circuit
b r e a k e r s . Most of the difficulties were caused by faulty test equipment and unrealistic
performance requirements rather than the breaker design. When the t e s t s were begun,
the b r e a k e r s consistently failed to pass the operational life test because of actuator knob
breakage. Reappraisal of the actual breaker use, however, indicated that the require-
ments were unrealistically severe. The breaker requirements were reviewed and then
redefined to establish realistic requirements, after which the b r e a k e r s performed
satisfactorily .
After a salt-spray test, a group of breakers was s e t aside for several hours
before being checked functionally. When the test was attempted, salt had built up be-
tw.een the actuator collar and the mounting sleeve to such an extent that the actuator
could not b e moved. This requirement was also determined to be unrealistic because
it w a s not representative of actual conditions. Therefore, the breaker was not consid-
e r e d to b e unsatisfactory.
15
Trip limits for the b r e a k e r s were selected without a c c e s s to performance data.
When tests were performed, many b r e a k e r s failed to meet specified values. A review
of t r i p limit values indicated that the specified limits were unrealistic and that breaker
performance w a s satisfactory under the redefined limit values.
During the Apollo 14 mission, a breaker failed to make contact when it was
mechanically closed. Postflight analysis disclosed a contaminant between the breaker
contacts. The contaminant was lost before it could be analyzed; however, the substance
on the contacts was probably bits of glass from a s m a l l fiberglass board inside the
breaker. Because this was the only known instance of this problem, corrective action
was not considered necessary.
Re1ays
Block I vehicles included an essential alternating-current DUS that w a s automati-
cally switched to the alternate s o u r c e if low voltage w a s experienced. Switching was
accomplished by using relays that were qualified f o r single-phase operation. However,
three-phase alternating current was being switched, which resulted in arcing between
the contacts and destruction of the relays. The possibility of the aforementioned
condition was not considered during the original p a r t s selection; as a result, a relay
capable of switching three-phase power was selected.
Relays were used in a cryogenic control box that w a s added to the vehicle during
the modification resulting from the Apollo 13 inflight problems. The original control
box was designed to have motor switches because they had no contact bounce, had high
current and voltage ratings, and were immune to vibration; however, as previously
noted, the motor switches were unsuitable for switching alternating current in a
vacuum. Consequently, when the additional box w a s designed, r e l a y s were used for all
switching functions.
16
,
Conformal coating of ladicote
over R N SAFETY MEASURES
Conformal coating of RlV 560-577 blend
i i 5;
on wire and terminal
A major consideration in the design of
the EPDS was the prevention of fault propa-
jacket
ll gation. Loads were placed on individual
circuits and isolated by circuit breakers,
Circuit breaker fuses, o r overload sensors. Buses w e r e
isolated with diodes and reverse-current
sensors. Maximum physical protection
was provided for boxes, components, and
wires to prevent damage during manufac-
ture, checkout, and flight. Closeout panels
and cable covers were used to shield the
equipment. Conformal coating was used
behind the panels and in other inaccessible
a r e a s . A typical example of the coating
applied to exposed electrical connections
is shown in figure 13. The coating not only
w protected the' system from shorts caused
PI jacket: Premolded polyimide glass jacket. Consists of three layers, each of
by floating debris but also sealed the com-
which is 8-mil glass cloth impregnated with polyimide resin and molded ponent against moisture and provided an
to a snug fit. Minimum thickness = 0.025 in.: used i n the CM crew
compartment as a fire retardant
inhibitor to prevent flame propagation.
R N 560-577 blend : Room-temperature-vulcanizing silicone rubber: used for
electrical insulation, moisture, and physical protection around the wire Wires. were especially vulnerable to
and circuit breaker terminal damage from overheating of adjacent
Ladicote A fire-retardant material for protection against burning i n pure wires because most of the wiring in the
oxyjen atmospheres.
vehicle is bound tightly in bundles. To
Figure 13. - Component coating. a s s e s s the reliability of the wiring and to
establish proper ground rules for harness
design, extensive testing was performed.
Wires were exposed to a variety of temperatures and p r e s s u r e s , some typical of those
that were anticipated and others in excess of what the w i r e s were expected to undergo.
Tests also were performed to establish the pertinent characteristics of the insulation
a t different temperatures. Data from these t e s t s were used to establish time limits
f o r various combinations of ambient temperature and p r e s s u r e for single wires and for
those in bundles.
17
RECOMMENDATIONS AND CONCLUDING REMARKS
The final overall design of the Apollo electrical power distribution system was
adequate. All the original concepts, however, were not satisfactory, as can be seen
in retrospect. Examples of some of the designs that were either modified or discontin-
ued are the automatic main bus disconnect, the automatic alternating-current overload
disconnect, and the inverter switching arrangement.
3. Some type of laboratory device (e. g. , breadboard, test jig, functional mock-
up, o r prototype) should be available for evaluation of the electrical power distribution
subsystem design early in the program and for u s e in providing real-time support
during missions. Several circumstances a r o s e during flight in which a dedicated device
for electrical power distribution subsystem simulation would have been helpful in
recreating problems and evaluating workarounds. The device, regardless of nomen-
clature, should be primarily f o r electrical power distribution subsystem support with
quick-change capabilities to keep the configuration current.
18
A realistic qualification program with rigid quality controls is necessary in the
selection of effective equipment. Comprehensive testing of each component and. of
higher assemblies is required. The experience gained from the performance of the
Apollo electrical power distribution subsystem should be used in the formulation of
guidelines f o r the design of electrical power systems f o r future space vehicles.