Place For Title: Resolving Cyclic Vibration On An Instrument Air Compressor
Place For Title: Resolving Cyclic Vibration On An Instrument Air Compressor
Nicolas Peton
Global Director, Machinery Diagnostics Services
GE Oil & Gas- Digital Solutions, Bently Nevada
Authors
• Amit Sharma
- Lead Engineer, GE-BN, Machinery Diagnostics Services, Abu Dhabi,
U.A.E.
- With GE-BN Machinery Diagnostics Services Group since 2007
- Project Engineer- Rockwell Automation-Entek IRD
• Nicolas Peton
- Global Director, GE-BN, Machinery Diagnostics Services, Nantes France
- With GE-BN Machinery Diagnostics Services Group since 2006
- Worldwide Startup Activities Site-In-Charge, Alstom (Steam Turbine) &
Cryostar ( expander/compressor)
- Operation & Maintenance Engineer- PPG Industry, USA
- Mechanical/Acoustical Research Engineer, Technion, Haifa and TU Berlin
Case Study on Resolving Cyclic Vibration on an
Instrument Air Compressor Train
Instrument Air Compressors are considered critical equipment in
the plants, supplying compressed air to the instrumentations in
the field. This case study focuses on cyclic vibration phenomena
observed in the 2nd and 3rd stages of an Instrument Air
Compressor, part of an Integral Gear Compressor train driven by
a motor. The machine train is equipped with an online vibration
monitoring and protection system with online diagnosis software,
which was used to diagnose the phenomena & forward path for
the resolution.
Content
• Problem Statement
• Machine Train Details
• Observation/Analysis
• Conclusions & Recommendations
• Machine Inspection Findings
• Corrective Actions / Lesson Learned
Problem Statement
• 3-stage integrally-geared instrument air compressor train
experienced cyclic vibration.
Critical Speeds
1st Stage - 21000 rpm
2nd /3rd Stage - 30800 rpm
Observations/Analysis
Direct & 1X Vibration Trend for 3rd Stage:
Steady
State
Transient
-Transient condition appears normal, where machine reached operating speed with
normal behavior
-1X Phase revolution occurs just after reaching operating speed during steady
state
Observations/Analysis
Transient & Steady State- 1X Polar Plots of 3rd Stage Bearing:
Transient
Steady
State
-Transient condition appears normal, where machine reached operating speed with
normal behavior
-1X Phase revolution occurs just after reaching operating speed during steady
state
Observations/Analysis
Shaft Centerline Plots
Suspected Reasons:-
• Carbon Seals rub due to mis-alignment across the gears.
• Burnishing is suspected due to shear stresses in the oil causing high
temperature.
Corrective Actions / Lesson Learned
Corrective actions:
All the pinion rotors were replaced with new rotors.
All the bearings were replaced.
Alignment of the integral gear assembly was carried out.
Lubricating oil was replaced per the recommendation from OEM. The oil
type was changed in terms of viscosity (higher to lower viscosity).
Lessons learned:
Oil degradation can lead to shear stresses in the oil lubricant. Hence
monitoring of oil quality is also an essential activity.
Availability of historical information from online condition monitoring
system enabled identification of the root cause.
Post Maintenance Data Plots
1X Polar Plots of 2nd and 3rd Stage bearings:
Stage 2 Stage 3
Stage 1 Stage 2
Stage 3