Design Operation of Full-Scale Anaerobic Dairy Manure Digester 1979
Design Operation of Full-Scale Anaerobic Dairy Manure Digester 1979
1 September 1979
Ecotope Group
2332 East Madison
Seattle, WA 98112
principal authors:
Elizabeth Coppinger
Jack Brautigam
John Lenart
David Baylon
David Smith
graphics:
Carol Oberton
‘Ihis report was prepared under contract to the U.S. Department of Energy,
Division of Solar Technology, Fuels from Biomass Systems Branch. The
content of this report, however. is solely the responsibility of Ecotope
Group and does not necessarily represent the views of the U.S. Department
of Energy. U.S. OOE Contr%ct 8EG-77-C-06-1016
REPORTON THE DESIGN
AND OPERATIONOF A FULL-SCALE
ANAEROBICDAIRY MANUREDIGESTER
1 September 1979
Ecotope Group
2332 East Madison
Seattle, WA 98112
principal authors:
Elizabeth Coppinger
Jack Brautigam
John Lenart
David Baylon .
David Smith
graphics:
Carol Oberton
This report was prepared under contract to the U.S. Department oi’ Energy.
Division of Solar Technology, Fuels from Biomass Systems Branch. The
content of this report, however, is solely the responsibility of Ecotope
Group and does not necessarily represent the views of the U.S. Department
of Energy. U.S. DOE Contract #EC-77-C-06-1016
.-
'TABLE GF CONTENTS
Chapter Page
Abstract ii
List of.Figures iii
List of Tables iv
Summary 1
Conclusions 4
I. Introduction 5
II. System Description 7
A. Introduction 7
B. Design 8
C. Tanks 9
0. Manure Handling System 9
E. Digester Heating and Mixing System 10
F. Gas Handling System 12
III. Operational Experience 14
A. Tanks and Insulation 14
B. Manure Handling 18
C. Digester Heating and Mixing 24
D. Gas Handling and Utilization 39
P
d. Start-up and Shutdown 46
IV. Biological Performance 49
A. Laboratory Testing 49
B. System Start-up 49
CC Gas Production and Digestion Performance 51
D. System Shutdown 54
E. Biological Stability 56
V. Net Energy 57
A. Overview 57
B. Gas Production 57
C. Energy Inputs 57
D. Net Energy Evaluation 58
VI. Economics 63
Appendix 1 72
Appendix 2 74
. .^-
ii
ABSTkCT
A full-scale anaerobic digester on the Monroe State Dairy Farm was operated
and monitored for 24 months with funding provided by the United States
Department of Energy, Fuels from Biomass Systems Branch. During the period
of operation, operating parameters were varied and the impact of those
changes is described.
Biological stability was monitored, and test results are given. Gas production
rates and system net energy are analyzed. The economics of anaerobic digestion
are evaluated based on various financing options, design scales, and expected
benefits. Under many circumstances digesters are feasible today, and a means
of analysis is given.
iii
LIST OF FIGURES
Number Page
Number Page
--
Ecotope Group has been under contract to the United States Department of
Energy to operate a full-scale anaerobic digester for dairy cow manure at the
State Reformatory Honor Farm near Monroe, Washington. The system was designed
by Parametrix Engineering and Ecotope Group under contract with the Washington
State Department of Social and Health Services (DSHS) and the State Department
of Ecology (ECOLOGY).
The Monroe digester provided a reliable source of fuel gas over the 23 months of
operation. The plant evolved during the two years of work, and is much different
from the original plan. It is more simple, easier to operate, and also more
energy efficient. The improvements for the most part were made by eliminating
equipment and operations that were found to be unnecessary. These improvements
have contributed to making the technology a feasible alternative for energy
production.
The digester design included a gas recirculation mixer based on sewage treatment
plant experience. This mixer, a Rootes blower, was expensive, requirrd considerable
electrical energy, and required regular maintenance, Use of the mixer was
progressively reduced from continuous operation to no operation at all. Experiments
showed that sufficient mixing occurs naturally in the tank, due to natural
convection currents and gas bubbling. No reduction in gas production or operational
problems resulted from the elimination of gas recirculation mixing. The electrical
energy savings were about 60 GJ per month, which represents about 90% of the original
electricity demand of the system and a significant portion of the net energy yield.
Thus savings in capital cost;operating cost, and maintenance cost for dairy
manure digesters can be achieved by simply eliminating in-tank mixing from the
design.
The biological stability of digesting dairy manure was impressive. There was no
need to alter the naturally occurring biological conditions throughout the 23 months
of operation. The contents of the digester were stressed by subjection to periods
without substrate loading during equipment outages, and to a fourteen day period
without heating or loading during shutdown. In all cases, gas production
recovered quickly upon resumption of loading and heating.
The gas handling system functioned reliably after an initial period of trouble-
shooting. The majority of gas handling problems were due to the high moisture
content of the gas, and to freezing of water condensate in gas lines during
winter. The problems were overcome by installing an adequate number of drip .
traps and insulating outside gas lines to prevent freezing. With regular
maintenance, operation of the gas handling system was trouble-free.
The potential annual total energy production of the system is about 1800 GJ.
The potential annual net energy yield is about 950-1000 GJ. Further improvements
in net energy would be possible by improving component efficiencies. The
influent/effluent shell and tube heat exchanger failed to recover effluent heat
as expected. Lack of forced convective currents in the flowing manure,
and the tendency of the manure to flow in stratifications inhibited heat transfer
in the flowing streams. The prospects for a successful shell and tube influent/.
effluent heat exchanger design are not good, and other methods of effluent heat
recovery are probably more promising.
The economics of dairy manure digester systems similar to the Monroe facility have
been analyzed based on various financing options, design scales, energy outputs,
and expected benefits. These analyses show that owner-financed systems can
produce energy at less than the present cost of propane or fuel oil. If farm
labor costs are discounted by assuming no additional hired labor is required,
energy can be produced at costs less than the cost of natural gas in many areas
of the country. If electricity is the energy output, all farmer-financed
systems analyzed can produce electricity for less than $.OSS/KWH. The analyses
show that energy produced by anaerobic digestion is competitive with many
present energy costs.
Anaerobic digestion of manure has often been considered of minor importance
in light of the national energy need. Widespread application, however, could
make farms and feedlots significantly less dependent on fossil fuels and make
them net energy producer:. This step would make agriculture less vulnerable to the
uncertainties of energy ~xpply and rapidly inflating energy costs.
CONCLUSIONS
The face of agriculture in the United States has altered dramatically since the
end of World War II. Technological advances, fueled by inexpensive energy, have
revolutionized agriculture in this country and made it the most technologically
advanced and productive in the world. Like other industries, agriculture has
moved toward centralization to improve productivity and profits. In livestock
operations, larger numbers of animals are being concentrated on smaller areas
of land. While confined herds have improved productivity and eased management
problems, they are completely dependent on mechanical systems to deliver food and
remove manure.
Although these developments have increased profits during the past two decades,
recent changes in water pollution legislation and the cost of energy have re-
sulted in increasing economic pressure on farmers. With the passage of the
Federal Water Pollution Control Act, and the subsequent regulations concerning
non-point source pollution, farmers are being required to deal with the wastes
they produce. Although regulations now seek voluntary compliance with the recom-
mended manure management practices, agencies will be given enforcement powers
in 1981 to insure that farms do have adequate manure handling systems.
The pressures concerning waste management are added to the rising costs of fuel
and fertilizer. The increasing cost of inorganic fertilizer is causing many
farmers to reconsider the use of animal manures to replace fertilizer now being
purchased. The rise in the cost of fuel is probably the.most dramatic and unanti-
cipated problem facing the farmer, Not only have inflation and fuel costs esca-
lated at a rate unforseen five years ago, but farmers are now beginning to fear
fuel shortages. In some areas, the diesel shortages of the summer of 1979 are
perceived as a precursor of serious future shortages. The idea of energy inde-
pendence is gaining wide appeal among farmers.
The economics of digestion for farm scale systems is improving, notably due to
rising fuel costs. Funds are becoming available for the construction of digester,s,
both as energy producers and as components of improved manure handling systems,
Federal and State programs to encourage the use of solar energy can also provide
valuable economic incentives for the use of anaerobic digestion.
All of these factors combined will very likely result in a tremendous growth in
the use of anaerobic digestion on farms. It is important that reliable and ef-
ficient systems be developed now that can operate on a farm scale. The research
conducted over the past two years at the anaerobic digester in Monroe has focused
on examining the problems encountered in operating a full scale system and on
improving the feasibility of these systems for farm use. Work has centered on
increasing system net energy, decreasing operator time, and improving system
reliability. The experience at Monroe has shown digestion to be feasible and
workable at farm scale. The information generated can be used to develop simple,
systems that can be integrated into farming operations. Operating demonstrations
of reliable, economical, and commercially available systems are essential for
anaerobic digestion to achieve its potential capacity to provide a significant
amount of energy to the agricultural sector.
7
II. SYSTEMDESCRIPTION
A. Introduction
A full scale anaerobic digester was built on the Washington State Dairy Farm in
Monroe, Washington, in January of 1976 by Ecotope Group of Seattle (Figure 1).
Funds for the digester were provided by the Washington State Department of Ecology
as part of a program to upgrade the farm's manure handling system for the purpose
of water pollution control. The system was run until May, 1976 and then shut down.
In June of 1977 funds were granted by U.S.E.R.D.A. to restart the digester, docu-
ment operation and maintenance characteristics of the system, and to prepare an
operator's manual that would allow the State to resume operation of the project.
The system was run continuously from August 1977 through August 1979 by Ecotope
Group personnel. The operation of the digester was taken over by the prison
system in September 1979 and the gas produced will be used to fuel the boiler in
the farm's creamery.
=*Incoming manure
EZZ*Out going manure
zz .Cold water
I. [ - l Hot water
-s".m Bio-qas flow
.I
The Washington State Dairy Farm is located 56 km (35 miles) north of Seattle, and
is operated in conjunction with the State prison system as a minimum security penal
institution with 30 inmates and 10 civilian employees. The 250-acre farm has 400
head of Holstein cattle, with a milking herd that varies from 180 to 200 cows, and
a creamery to process milk, cottage cheese, and ice.cream for use in government
institutions (Figure 2).
SITE
for PLAN
1 METHANE DIGESTER
MONROE, WASHINGTON
n
key
TllhSFL”
P"IP
.. e - lab Irailer
The milking animals are housed in a covered loafing shed with a concrete floor
and individual sawdust-bedded stalls. Only the manure from those animals in the
loafing shed is used in the digester.
B. Design
The Monroe digester was designed on the model of a municipal sewage treatment plant
digester, and was a transfer of state-of-the-art treatment plant technology to an
agricultural application. During the design phase of the system, an emphasis was
placed on the use of off-the-shelf components that are easily obtainable. It was
felt that using equipment already proven and accepted in the agricultural sector
would speed the widespread use of digestion technology. The system consists of
four major subsystems: the digestion tanks, the manure handling system, the
digester heating and mixing system, and the gas handling and utilization system.
The components of each subsystem were chosen on the basis of commercial availa-
bility, cost, proven effectiveness, and energy consumption.
C. Tanks
The digester tanks are an example of the integration of agricultural sector products
with sewage treatment technology. The reactors are two 189 m3 A.O. Smith Slurry-
store tm tanks fitted with Harvestoretm silo roofs. These fixed cover tanks are
7.82meters in diameter and 4.57meters in height. The tanks are glass-lined
steel tanks that are built to be corrosion resistant. Certain modifications are
made to the tanks for use as experimental anaerobic digesters. In addition to the
Harvestore manhole covers added to the roof and sides of the tanks, two thief holes
were installed on the digester roof for sampling digester contents from the tank
interior. Eight side-mounted sampling ports were installed at three levels around the
perimeter of the tank to provide a variety of sampling locations.
The most significant tank modification was the insulation of all exposed tank
surfaces. The interior roof of the tank was sprayed with 8.8 cm of polyurethane
foam (R-12). Exterior walls were covered with 10 cm of Dow Styrofoam SMtm (R-22),
and covered over with corrugated galvanized iron roofing sheets.
The digester was designed to integrate into the farm's existing manure handling
practices. The concrete cznter aisle of the loafing shed was extended out the
south side of the shed, and a concrete tank with an iron grate-covering was built
at the end of the aisle (Figure 3). Each morning manure is removed from the
loafing shed by a tractor with a rear-mounted scraper. Since manure is scraped
only once a day and includes sawdust and woodchips used for bedding, it often
contains thick clods of manure and is drier than a pure, continuously scraped
substrate. Water is added to the manure in the influent tank, and the contents
are mixed with a 7.46 kw centrifugal chopper pump with a 5 cm iron pipe by-pass on
the discharge line. To provide mixing of the slurry, manure is pumped from the
bottom of the influent tank and discharged through the by-pass pipe that is aimed
at the surface of the manure. The pipe is moveable and can be directed to areas of
the tank that require mixing. Either the chopper pump or a variable speed pro-
gressive cavity pump is used to load the slurry into the bottom of the digester.
As manure is loaded into the bottom of the digester, the liquid level in the digester
rises and manure is displaced through an overflow pipe at the top. From there it
flows into a storage lagoon, and is eventually applied to the field with spray guns.
The manure is used to fertilize crops grown for cattle food.
Because of the emphasis placed on the use of commercially available equipment, only
two pieces of equipment were specially fabricated for the project. One was an
influent/effluent heat exchanger, and the other was a draft tube heat exchanger
that constitutes the core of the digester’s mixing and heating system (Figure 4).
The draft tube heat exchanger consists of two connected concentric cylinders of
galvanized metal through which hot water flows. The digester operates at 35’C.
Hot water is circulated through the internal heat exchanger from either the boiler
or from the coolant system of an internal combustion engine that burns biogas to
produce electricity. The heat exchanger doubles as a draft tube for use in
conjunction with the digester mixing system.
Because of scum formation problems experienced in municipai sewage treatment plants,
the Monroe digester was designed to be continuously mixed by gas recirculation.
GAS -,
WATER z
_I-.-.
According to the original design, gas was to be either burned directly in the boiler
for heating the digester, or scrubbed and stored for later use. The primary use for
the gas was burning in order to produce process steam in the farm% creamery. It
can also be used in an internal combustion engine to produce electricity in emergency
situations.
_
Fig. 6 Gas Handling System
l’he low pressure system was designed to meet the ccnstraints of the upper and lower
pressure limits of the digester tank. The tank was pressure tested to 4.9 kPa.
Pressure relief valves were set at 0.S kPa vacuum and at 2.7 kPa positive pressure.
As gas is produced, it will first be available to the boiler. If the digester
thermostat indicates heat is needed, the boiler will turn on and burn raw biogas.
Once the digester is brpught yp to temperature, the boiler will shut off and the gas
pressure in the system will rise. When it reaches 2.4 kPa, a compressor is activated
if storage tanks are below maximum pressure 1.65 MPa. a
If system pressure falls below 1.7 kPa, the compressor will shut off to prevent re-
ducing the system pressure to below satisfactory limits. When the gas storage tanks
are up to pressure, the compressor will shut off and system pressure will again rise.
When it reaches 2.7 kPa, a flare is activated and will run until system
pressure is reduced to 2.4 kPa; If the pressure goes above 2.7 kPa, a relief
valve on top of the digester will release gas. There is also a back-up
pressure relief valve set at 4.0 kPa. When both of these relief valves fail,
tank contents are forced out through a 1S cm diameter PVC overflow pipe on the
effluent line.
Three 3.79 m3 propane tanks are used for storing biogas. . These tanks have a working
pressure of 1.65 MFa and are capable of storing 62 m3 of gas each. A Corken two-stage
compressor with a 1.5 kw motor is part of the storage system. Gas that is com-
pressed first passes through a hydrbgen sulfide scrubber to extend compressor life.
.-. -
An internal combustion engine with a 40 KVAS_(peak)-generator was installed.
.
as a part of the original demonstration project. The purpose of this installa-
tion was to provide emergency back-up electricity for the creamery and milking
operations. Because it was sized to meet peak electrical needs and not to be
compatible with daily gas production rates, it required a gas storage system.
The engine is a Waukesha VRG 310 natural gas engine with a dual fuel Impco Model
200 carburetor. The engine is directly coupled to a Kato generator. When the
,I.C. engine is operated, waste heat from the coolant system car. be circulated
through the upper portion of the heat exchanger.
G. Monitoring Equipment
The digester was outfitted with monitoring equipment to assess system performance
and energy production. Gas meters were installed to measure gas production and
consumption of the boiler, the T.C. engine, and the flare. Electric meters were
installed on pumps, the mixer, and the I.C. engine. Temperature probes were
installed at a variety of locations in the tank to monitor material and heat
movement within the tank. A laboratory was also installed at the site to monitor
the biological health of the system. I
The system has been operated and maintained for two years. The biological
stability and handling characteristics of dairy manure differ so significantly
from municipal sewage that many of the original design assumptions were incorrect.
Anaerobic digestion of dairy wastes is simpler and more Reliable. Systems designed
on a smage treatment model will be oversized, inefficient and prohibitively expensive.
The information gained at Monroe can be used to simplify and correctly design
anaerobic digestion systems for dairy farm operations.
15
III. OPERATIONAL
EXPERIENCE
The digester at Monroe ccnsists of four subsystems: the digestion tanks and
insulation, the digester heating and mixing system, manure handling, and gas
handling and utilization. Operational experience with each of these subsystems
has provided information on how to reduce the capital cost of a digester by
.
eliminating unneccessary equipment, decrease operator time and maintenance cost,
and improve the net energy of the system.
1. Corrosion
The A-0. Smith Slurrystone tanks are constructed from glass lined steel sections.
One of the tanks had been in continuous operation for two years, and was recently
emptied and examined for corrosion. No corrosion was evidenced on the interior
walls, or on any of the plastic coated bolts used to fasten sections of the wall
together. 'There was corrosion on one of the untreated bolts used to install
sample ports. Significant corrosion was occuring on the fastening bolts on the
exterior of the tank. A number of bolts on the roof were rusted. The most consis-
tant occurrence of corroding bolts was near areas with known small gas leaks such
as thik:f holes and the pressure relief valve. The mixture of biogas and oxygen
appears to be much more corrosive than just oxygen. The limiting factor in the life
Of the tanks seems to be the lifetime of the nuts and bolts. During construction,
nuts and bolts should be protected from corrosion by covering them with a tar-plastic
compound.
2. Cleanout
When designing a rigid tank system, provisions should be made for periodic removal
of grit accumulation. Frequency of cleaning can be reduced by removing as much
grit as possible from the manure before it is pumped into the digester. Agitation
inside the tank can help keep the grit in suspension, but there is a high energy
cost for such mixing. There will still be some grit accumulation, however, even
with attempts to reduce it. Options that will allow grit to be removed without
shutting down the digester are preferable because of the difficulty and danger
associated with shutting down a digester. A sloping floor that consolidates the
grit and an auger system to remove it is one possible solution for periodic clean-
outs of grit.
The Monroe tank had no such provision, but was equipped with a 30 cm drainwhich
allowed the digester to be emptied into the effluent tank. There is also a man-
hole in the sideof the digester that allows access to the tank. The30 cm drain
allowed flushing out the solid organic material remaining in the tank after
the fluid was removed. Some of the sand was also removed this way, but it re-
peatedly clogged the lines and was more difficult to remove from the effluent tank
than from the digester.
Ultimately, the grit had to be shoveled out of the digester through themanhole
opening. This was a verylaboriousand time consuming job, and is one of the
least preferabl e options for grit removal. If a digester is designed for manual
grit removal , .tank openings should be located in an area that has easy access for
a wheel barrow and be of sufficient size to allow for easy entry and exit of the
digester.
3. Insulation
Three types of insulation were used on the digester :polyurethane foam, beadboard,
and blue Styrofoam. The polyurethane foam was applied to the interior of the tank
roof to allok easy access to exterior roof bolts, in case of a gas leak. It was
the most expensive type of insulation used. Polyurethane was chosen because only
a spray of insulation could be applied to the interior of the roof. After two
years of contact with manure and biogas, there was no evidence of significant
degradation of the insulation.
The exterior walls of thetank were originally covered with headboard insulation.
The beadboard was then covered with tar. Although the insulation was relatively
ipexpensive, it was not adequate. The rainy climate of the Pacific Northwest
17
resulted in the beadboard absorbing water and losing its insulation value. The
beadboard was then removed and replaced with blue Styrofoam. Four inches of
T. & G. blue Styrofoam were applied to the tank in &gust of 1977. It was covered
with corrugated sheet metal. This insulation was approximately 50% more expensive
than the beadboard but has worked much better. No problems with water absorption
have been found.
B. Manure Handling
1. Introduction
Probably the most difficult aspect of operating the digester at the Monroe facility
is manure handling. Traditionally, this has been one of the greatest problems
facing dairy farmers. Commonmanure handling problems, such as pump perforriYlnce
and maintenance, and clogging of pipelines, are compounded in a digester systei;b
owing to the thicker manure slurries handled. Thicker slurries are desireable
because they result in reduced digester heating demand. Obviously, there is a
I trade-off in gas heat energy, and pumping and mixing operating and maintenance
costs.
A dirt feedlot scraped out only occasionally demonstrates two points. First,
the manure will have undergone partial degradation and will not produce as much
gas as fresh manure. Second, the dirt and other debris scraped with the manure,
if not removed, will gradually fill in the digester, reducing its effective volume
and possibly causing clogs.
A manure washdown system illustrates a third point. This manure is usually too
watery for efficient digestion. Water with the manure must be heated to the
digester temperature, thus consuming gas, but not lending to increased gas pro-
duction. A more dilute digester slurry also requires a larger digester volume
adding extra capital cost co the system.
Finally, bedding, such as woodchips or straw, can both clog in certain pumps and
pipes and contribute to a rapid scum layer build-up if it floats. To minimize
this build-up, which can retard gas production and cause effluent clogs, mechanical
or hydraulic mixing can be used, but at added capital and energy expense. Another
possibility is to maintain a thicker digester slurry so that material that nor-
.
mally floats in a thinner liquid will remain in suspension.
I
a. Pipe Clogs
Pipe clogs have demanded an excessive amount of attention at the Monroe facility.
To minimize clogs, it is best to understand the different ways that they occur,
so that potential clogging conditions are eliminated by design. The most obvious
clogs are those caused by a large particle or object either partially or completely
blocking flow. Smaller particles will catch and build on the immovable ones, worsen-
ing an alre&y restricted flow situation or halting flow completely. This type
of clog is most commonon raw manure influent lines containing foreign materials.
Rocks, knots of wood, cow tags, bailing wire and aluminum cans have been found to
block a 5 cm diameter line used for influent mixing. The problem is much more
acute at the point where material enters this pipe from a 10 cm diameter line and
at a 5 cm diameter elbow. In an otherwise "cleanl' raw manure stream, bedding,
feed pellets, and dried clumps-of manure have also clogged 5 cm diameter pipe.
Small pipe diameters and large reductions in pipe diameter on hydraulic mixinga&
loading lines should be avoided. Up to % hour or more may be spent freeing just
one clog, if manual removal and freeing of pipes is required. This sometimes
involves climbing down into the influent mixing tank. Ordinarily, flushing with
a stream of high pressure water:will dislodge a clogged line, although if back-
flushed, there is no assurance that, the line will not become clogged with the same
material again.
Raw manure, and less frequently, digested manure, when left remaining in pipes
long enough, begin, to thicken and "cake". If lines are not used daily, they may
require flushing out with water to prevent this type of clog. This effect was
much more evident in flexible hose and occurred even in 10 cm diameter sections.
The evaporation or leaking of water from the slurry contributes to this effect,
leaving a drier material behind to cake. This type of clogging is usually dispersed
by an increase in gravity or pump head. A water flush can also sometimes be useful.
Heavier solids such as sand or gravel settle out of watery manure slurries. The
digester has illustrated this process; after two years of operation, almost 30 cm
of sediment was found on the digester floor. Practically all pipe clogs of this
nature were in the effluent lines, since digestion reduces solids levels approxi-
mately 30%. The percent total so1ids level of raw manure loadedis normally 10% TS;
that in the digester and effluent is about 7.5-8% TS. Most settling clogs in
effluent lines have been noted at solids levels below 7.5% TS, the lower level due
to boiler or fresh water leakage, or dilute slurry loading to the digester.
Settling clogs only form in horizontal pipes and at low velocities. In an effluent
section where the pipe diameter reduces to 7.5 cm from 10 cm, sand deposited in and
blocked only the 10 cm section. In the 7.5 cm line there was sufficient velocity
to keep the sand moving in suspension. Large pipe diameters and pipe reductions
on horizontal effluent lines, therefore, should be.avoided. Settling clogs are
best removed by high pressure water or air.
3. Pumps
Successful pump selection is a major component of the efficient manure handling
system. A pump should not only be properly sized but suited to handle the nature
of the substrate at hand. Along with a manure slurry, there may be bedding, gra-
vel, or other foreign matter that must be accounted for.
Before selecting the best pump for a job, the decision should be made whether a
pump is needed at all. In the case of transporting digested effluent, at the
Monroe digester, this stream is now moved over 50 meters from the digester to the
holding lagoon by gravity. About 4.5 cm of static head is available for this
purpose using 10 cm diameter vertical PVC pipe and 7.5 cm diameter horizontal
PVC pipe. Digested manure is a :far more homogenous fluid than raw manure, and
for this reason, causes far fewer clogging problems in smaller diameter pipe.
Loading raw influent to a digester by gravity is not a simple matter. Raw manure
does not flow well if very thick or not well mixed. This is an area that needs
further investigation. At the Monroe facility, three pumps have been tested
for loading in various ways. Of these, one pump also mixes the influent. An
independent mechanical mixer has also been tested as a possible improvement.
A centrifugal chopper pump (Vaughan Co., Inc.) was intended to mix the influent
by chopping and recirculation, but it is also able to load. Manure is mixed by
two separate means operating simultaneously. The centrifugal impeller chops up
any manure clumps that it draws in from the tank bottom. Also, a movable recycle
pipe on the discharge line of the pump is aimed at the slurry surface, and a high
pressure slurry stream provides overall circulation of the tank contents. Since
the tank is square, large clumps may sometimes get stuck in the corners which
requires manual directing by an operator with a pole. Most large clumps float,
due to encapsulated air and are broken up by the surface recycle stream.
Centrifugal pumps are designed for high volume, low pressure service. Smaller
sized pumps may possibly develop too little pressure for handling thick slurry.
A large*pump may load manure too rapidly. At Monroe, a rapid loading rate caused
21
gas to be forced out through the press&e rel ief valve. Valving down flow is
limited because reducing the diameter of the valve caused clogging. The centri-
fugal pump at Monroe is driven by a 7.5 kw motor. The mixing tank is approx-
imately 3.7 meters square and 2.4 meters deep. At these specifications, and with
the existing mixing capability, lO%TS has been the practical limit for easy
mixing and pumping. At 12% TS, mixing becomes labor intensive and pumping is -
severely limited.
A--.progressive cavity pump (Moyno Pump Div., Robbins and Myers, Inc.) was obtained
to replace the diaphragm pump. It also works on the positive displacement prin-
ciple, but does not use check valves. Instead, a single. helix rotor revolves
within a double helix stator forming cavities that progress toward the discharge
end carrying the substrate w;th them. The pump cavities were sized to handle
particles up to 2.8 cm, and a variable speed drive with an 11.3 kw motor was
selected for delivery of from 2-5 m3/hour at up to 700 kPa. High pressure capa-
bility was desirable to insure loading thick slurries through an influent/effluent
heat exchanger of unknown pressure loss. Variable speed was desirable to optimize
heat exchanger performance.
The Qne significant operational problem related to this pump was finding an ef-
fective means of removing large foreign objects from entering the pump. A clog
at the volume reduction from suction housing to cavity may cause the pump to run
dry, which leads to burnout of the stator if not quickly detected. A most crude
filter on the suction pipe (5 cm square openings on a 15 cm diameter line), and
an automatic shutoff switch sensing low flow conditions, were installed to safe-
guard the pump. The in-line filter invariably clogs due to thick slurry or foreign
matter, and requires cleaning. The shut off switch has several times proved un-
reliable. This pump was able to load a thick slurry, but the performance of this
pump exceeded mixing limitations. Up to 13% TS were pumped, but at this solids
level, mixing was practically impossible with the existing chopper pump and re-
cycle stream. This pump has not been run since the removal of the influent/effll:. ,t
22
heat exchanger and return to 10% TS loading, which the centrifugal pump handles at a
much faster rate.
Amechanical mixer was designed to stir the contents of the influent tank that
incorporated mixing blade, shaft, support structure, and 5.6 kw motor. This
device has definite potential if prooerly sized. There are no clognine problems
to soeak of. The unit that was tested appears slightly undersized for thick slurries
of over 10%TS. Mixing of the raw influent would also be easier in a circular,
rather than square, mixing tank.
There are trade-offs between the energy gains that result from increasing the
percent solids loaded, and the electrical and labor demands of an influent
handling system. The characteristics of manure slurry differ so significantly
as the percent solids are rais.ed, that an influent handling system should be de-
signed for the specific requirements of that solids level that provides the most
cost effective and energy efficient system possible.
I J
IUFLUZNT TANK
23
The results of the tests, conducted during June 1979, were AP's ranging from
0.048 to 0.176 kPa/m over velocities between 0.085 and 0.76 m/s and TS between
9.2 and 12.5%. The AP'.s determined are comparable to those calculated using
formulas devised by Hashimoto and Chen (published by ASAE, 1976), from 0.055
to 0.143 kPa/m for TS between 8.6 and 11.4%. The results indicate there is no
corre;lation between AP and velocity over the range tested. There is a gradual
but significant increase in AP with %TS. This relationship is shown in figure 9.
When designing manure handling systems for slurries of 12% TS, for example, AP's
may increase 13-3 time s over 10% TS or 3-6 times over 8% TS. This effect is
more pronounced with long pumping distances and increased numbers of bends and
valves. ~ With thicker slurries, shorter pipes and fewer fittings should be used
.
to limit the size of pump necessary.
_ - -.-.
0 . I I I I
8 3 la ii IZ I3
‘.TS
/
Figure 9 - Pelationship between pressure loss
and %TS
C. Digester Heating and Mixing
1. !ikating
The contents of the digester must be maintained at about 35°C to produce gas at
the optimum rate. This requires a daily heat input to counter digester heat
losses from two sources: 1) conduction skin losses and, 2) displacement of warm
digested manure by cold influent. A significant portion of the daily gross gas
production is needed to maintain digester temperature. Heat transfer in the tank
is accomplished by the draft tube heat exshanger.
Heat loss through the skin is determined by the heat transfer coefficient of the
digester surface, the surface area available for heat transfer, and the temperature
difference between the digester contents and the outside air. All exposed surfaces
af the Monroe digester were insulated. Ten centimeters of Dow Styrofoam SMtm
dere installed on the exterior walls, and about 8 cm of polyurethane foam was
sprayed on the inside of the roof. The observed heat loss rate from the insulated
tank was about348 W/hrOC at an ambient temperature of 0.7'C.
[nfluent heating is by far the dominant factor in digester heat demand and accounts
For 75-90% of the total heat demand depending on the season. The amount of heat
necessary to raise the influent to 35'C depends on the volume loaded, the percent solids
WSI , and the influent temperature. The influent heat demand can be significantly
reduced by increasing the percent solids of the slurry loaded. This reduces the
unount of water added to the manure that must be heated to 35'C in the digester.
hoer the two years of piant operation, the percent soiids of the influent has been
increased from 4% to 10%. The reduction in the amount of water also improves gas
rroduction because it effectively increases the retention time of the organic material
.n the tank.
2. Boiler
rhe heating system boiler is a National 209 Series boiler with a rated output of
39(jMJ-'lhr; Dnsc-rubbed biogas is burned directly to produce-49'C water that is Pumped
into the bottom section of the draft tube heat exchanger. Operation of the boiler
is controlled by thermostats. A schematic of the boiler heating system is given
in figure 10.
%e efficiency if heat delivery from the boiler determines the gas consumption of
:he system. Calculations indicate that our boiler heat delivery efficiency is in the
25
The original temperature measuring and controlling devises for the heat delivery
system were all of mechanical design with capillary tubes from the sensor to the
switch. One probe was connected to a misroswitsh that controlled the digester
temperature by turning the boiler water pump on and off. The other was connected
to a meter calibrated in l.l°C increments. The sensors were mounted in two sep-
arate wells in the side of the digester.
The temperature control had a l.l°C bandwidth for turning the pump on and off.
The gas consumption of the boiler was very erratic on a day-to-day basis, and the
hot water pump often stayed on for many hours longer than necessary. The reading
of the temperature indicator also varied several degrees on sunny days. From this
information it was decided that a more sensitive and accurate temperature control
.-
would be needed. A combination temperature control and measuring unit was designed
and instalied. Its on/off bandwidth could be varied from 0.1 to 1.5'C; it was
set to 'O.lOC. This stabilized the temperature of the digester and resulted in
the ability to predict gas consumption on a daily basis given loading volume and
temperature.
_-
;..*
5. -‘t.
‘* i.,
-- ,’
-, i-’
- ‘.
.’ -_ ‘..
. . r ----- - ,-, *cI. --.-.& --.-+‘,;. ---
-.---
efficiency for electricity generation, since it replaces the need for boiler
heating. Efficiency would not be as good if the engine were run for 24 hours
because not all the waste heat would be needed for digester heating.
The problem with heating a digester with engine coolant is the prospect of over-
heating the contents with adverse effects, on the microbial population. If this
method of heating is used, a reliable thermostatic control of the flow of cooling
water to the digester is essential.
.
Figure 12 - Digester Heating System
.. . _-
It is of interest to determine the film coefficient orb the slurry side of the heat
exchaneer. To accomplish this, the water side coefficient was first estimated
using a well known Nusse IF-type equation. The equation for the overall heat
transfer coefficient could then be solved for the slurry side film coefficient
,2 0
yeilding a value of 3.78 MJ/hr-m - C. A comparison of the water side and slurry
side film coefficient shows that about 2/3 of the resistance to heat transfer is
on the slurry side (See appendixtfl).
The galvanized draft tube heat exchanger corroded in areas in contact with hot
water from the boiler or I.C. engine. The zinc coating was black, brittle, and
flaking in the worst areas. Areas not contacted by the hot water, such as supports
were not affected. It is clear that corrosion of galvanized metals immersed in
digesting manure is accelerated at temperatures above 35'C.
Figure 13
Influent/Effluent
Counterflow
Heat Exchanger
_ _.-.-.. _^. - *’ , c
5. Influent/effluent heat exchange
The unit was operated in February 1976, using a 3% TS slurry, but severe
clogging of the tubes occurred. Failure of a number of the tube connectors
resulted in short circuiting between influent and effluent, The segmented
aluminum tubes were replaced by single length thin wall PVC pipe in Oct. 1977.
This reduced the expected overall heat transfer from 58 to 50% (with 35' C
effluent and 10' C influent) at 1.0 m3/hr flow rates, but eliminated the
connectors. At 8% TS, the diaphragm loading pump continuously lost prime
due to improper check valve seating, and was not able to move slurry through the
heat exchanger. The centrifugal chopper pump was sometimes able to do so but
with inconsistent flow rates, therefore heat exchanger performance testing
under these conditions was unsatisfactory.
Beginning in March 1979, a progressive cavity pump was available that could
dependably load high solids through the heat exchanger at low flow rates.
Experiments indicated that practically no heat was exchanged in the heat
exchanger. Flow was varied between 4 and 6 m3ihr. influent TS ranged from
10 % - 13%, and effluent from 7 4 - 8 $%. Two basic problems were isolated
that account for the failure of the heat exchanger.
The first problem was stratified flow. Even after several hours of effluent flow
in the shell, about 50% of the heat exchanger shell surface area remained cold.
Assuming that thermal stratification is a sign of flow stratification, it is
obvious that only a limited surface area was available for heat exchange.
.
31
6. Digester mixing
Based on municipal sewage treatment problems with scum formation, the Monroe
digester was designed to be continuously mixed. A Rootes-type recirculation
blower was used in conjunction with an internal draft tube that doubled as the
system's heat exchanger. During the first five months of operation in 1977,
the blower ran continuously. The electrical demand of the blower was 180 klVh
per day, representing 90% of the total electric demand of the system. The
blower also required costly repairs during the time of its operation, as well
as routine oil changes each week.
The natural mixing that occurs is due to gas movement and thermal convection
currents from the heating system. Figure 14 shows movement from convection
currents established when the boiler is running. At.2 a.m., the temperature
throughout the digester was uniform. It had stabili,zed after the previous
day's loading, and the boiler had remained off for most of,the night. When the
boiler turned on, agitation could be seen at the three probe points. The spikes
on the chart represent manure that heated above the temperature of the rest of
the tank moving past the stationary probes. The decrease in the number of the
spikes from the middle to the upper probe indicates that the manure is losing
heat as it rises. The small temperature difference noted by the lower probe
may indicate that the manure passing it is replacing the manure that has been
warmed by the internal heat exchanger. This movement continued while the boiler
was on and decreased after the boiler shut off. Because we have not yet been
able to perfect a flow probe that can be inserted into our sampling ports, we are
unable to detect any mixing that occurs isothermally.
The impact of natural mixing with the boiler on during loading can be seen in
Fig. 15. The temperature of the digester contents was relatively uniform before
cold manure was loaded on the bottom. The drop in temperature at the bottom
probe shows the buildup of cold manure, Sharp spikes of low temperature at the
TOP PROBE MIDDLE PROBE BOl’TOMPROBE
3. lm above 2.lm above l.lm above
TIME digester floor digester floor digester floor
g:oo
baL=
OFF
2--
7:OO ___-_ i ..-_.
&xx I
50~
4:m
3XlO
z:oc
Figure 14
Temperature Probe Readings
34
IZ I=
8:oc
4:oo
-&s
-zL-
STef- LbAD-7
-_---- / -
=I-fZMfEk3J-U~ - C-
Figure 15
Temperature Probe Readings
,I
.,~
p /
I”
--
35
upper probes indicate cold manure was passing by. These probes are located
at 2.1 m and 3.1 m above the bottom of the tank. .Mixing could be seen for
about 10 hours after loading. Warm spikes predominate after the cold manure
d SM.
was heated and intermixmA
Figure 16 shows the impact of doub!.ing the heat exchanger area. In this case,
heat was provided from both the boiler and the I.C. engine. The effect of this
heating configuration is an increase in the speed of mixing. Even though the
size of the load is slightly larger than the previous example, the accumulation
at the bottom probe is less and the raw manure is mixed in rapidly. Hot spikes
predominate throughout, indicating that raw manure was warmed as it was mixed.
Mixing of freshly loaded manure, when the effects of convection currents and
gas bubbling are minimized, can be seen in Fig. 17. Convective mixing was
minimized by not heating with the boiler or I.C. engine, and by loading the
cold manure influent into the bottom of the digester tank. The mixing effect
of gas bubbling was most likely minimized, since it is expected that most of the
gas bubbling occurred above the accumulation of manure on the tank bottom. The
cold manure was distributed slowly throughout the tank, drawing the overall tempera-
ture down as it mixed.
In contrast to Figure 17, the effect of loading the digester to the top is shown
in Figure 18. In this case, mixing that resulted from convenction currents and
gas bubbling was optimized. The cold manure was mixed
. by convection as it tended
to settle toward the tank bottom, and was also mixed by gas bubbling during its
downward motion. Once again, the boiler remained off, however, the cold manure
almost completely mixed into the warm manure in only about six hours.
The indications from the studies and gas production data are that in-tank mixing
equipment can be eliminated from dairy manure digester designs. Natural
mixing from convection currents and gas bubbling can sufficiently mix the digester
contents. More rapid and thorough mixing can be achieved if manure is loaded
to the top of the digester, because the effects of convective mixing and gas
bubbling are optimized. Problems of scum formation can be eliminated simply by
keeping the % TS of the digester contents above the point at which scum layer
formation ceases to be a problem.
36
3:oo
ZAM
9:oo
b:oo
3:oo
5TAkZ-
U’AW
---_- !L --
32’
T~PE~ATUR~ - c”
Figure 16
-.-.-.-
-_---_
T&MPUrATU~- Co
Figure 17
Temperature Probe Readings
38
The elimination of in-tank mixing systems has a great impact on the economic
feasibility of digestion. It reduces capita;, energy, and maintenance costs.
It also reduces the vulnerability inherent in having equipment inside the digester
tank.
93x3
t -mPulu7
3:oo <
-e-v-.- --- .-*-. --_
, ST- WQ
12ffi %
-e-m-_- ---_ ---e-m----
I I I I . l 1 I
L
I
30” 32’ 3z” 3p
Figure 18
1. Introduction
Biogas has approximately 600 9 of the heating value of natural gas. It has
various potential household and farm uses such as cooking, water heating, space
heating, refrigeration, grain drying, irrigation pumping, food processing, and
electricity generation. Its use as a vehicle fuel is limited by the difficulties
of gas storage. Storage as a liquid requires expensive equipment, and storage
as a gas requires large volume even at high pressure (1.65 M?a). At present,
farm-generated biogas utilization experience is meager, although biogas utilization
at sewage treatment plants is relatively common.
A number of unanticipated problems were encountered with the gas handling system
during the start-up phase. The majority were due to the high moisture content of
the gas. Upon correction of the problems, the gas handling system functioned
reliably and, with proper maintenance, presented no problems.
Water condensate accumulation in the gas lines and meters caused numerous gas .
flow stoppages during the start-up phase of operation. The problem was solved
by installing manually operated drip traps at low points in the lines and at the
bottoms of meters. The drip traps are emptied daily, draining about 2 liters of
water from the system each day. Installation of an adequate number and regular
use of drip traps is essential to eliminate condensate blockages in a low pressure
system.
During the first winter of operation, water condensate froze in the gas lines and
meters, stopping gas flow. ,Freezing was a particular problem at the first v&lve
downstream of the digester in the low pressure piping. This ball valve is a line
restriction and causes the gas to drop in temperature-and pressure asit flows
through. The gas at this point has its highest water vapor concentration, and
the drop in temperature and pressure causes rapid condensation and enhances *
freezing in cold weather. Freezing problems were solved by moving the gas meters
into the warm boiler room and insulating the gas lines outside. Particularly
heavy insulation was placed around the ball valve that was usually open and did.
not need to be operated under normal conditions. These measures were sufficient
to prevent further freezing problems. It should be noted that freezing of gas
handling equipment can be a very serious problem. Twice during the first winter,
both the gas lines and the pressure relief valve at the digester top froze,
causing pressure to build up in the tank. The overflow design of the effluent
system provided back-up pressure relief since manure, and finally gas, was forced
out the overflow as pressure in the tank increased. Had this back-up pressure
relief not been'available, rupture of the tank might have occurred. Back-up
pressure reiief is an important advantage of an overflow system.
41
Problems were encountered in the high pressure (1650 kPa) system due to grit,
water, and oil in the gas lines. No drip traps were originally installed on the
high pressure lines, and water and grit accumulated for over a year eventually
causing the pressure reducers to malfunction. This problem was solved by taking
apart and cleaning the pressure reducers, and regular draining, of the water by
inserting a pressure gauge needle adaptor into a Pete's Plug. This removed water
without depressurizing the lines. An oil leak in the compressor caused oil to be
sprayed into the high pressure lines where it formed an emulsion with water in
the orifices and diaphragms of the pressure reducers. The reducers malfunctioned
causing the downstream low-pressure line to increase in pressure from 14 kPa to
172 kPa, and gas was vented through a pressure relief valve. This resulted in
a significant gas loss for about a week. Cleaning the emulsion from the lines
and reducers returned the system to normal functioning.
42
These experiences indicate the need for regular water removal from gas lines and
a bi-yearly cleaningof the high pressure lines to remove grit and oil-water
emulsion. The bi-yearly cleaning takes approximately four hours in a regular
maintenance schedule. Our experience with moisture condensation in the gas lines
led us to believe that a large amount of water had probably condensed in the
storage tanks, however, only 0.6 cm of water was found at the low points of the
tanks.
5. Utilization
Biogas was used at the Monroe digester to provide fuel for the heating system
boiler, lab-trailer, and internal combustion engine. The original plan was to
size the gas to fuel a boiler in the farm creamery, however, funds for pipeline
construction were not available until the fall of 1979. Gas production in excess
of needs at the digester site was flared. The digester boiler burned unscrubbed
biogas..The only noticeable difference from burning natural gas was the need to
clean sulfur deposits from the burner jets every six months.
The internal combustion engine and generator were installed as part of the original
demonstration project. The purpose of the installation was to provide emergency
back-up electricity for the creamery and milking operations. The engine is a
Waukesha VRG310 natural gas engine with a dual fuel Impco Model 200 carburetor.
The engine is directly coupLed to a Kate 40 kVA (peak) generator. Engine cooling
water can be circulated to the internal draft tube heat exchanger to provide
digester heating. A Westinghouse D4S-7 kilowatt-hour'meter ,was used to monitor
the power generated.
Bituminous coatings are available from pipe vendors and protect the pipe from con-
tact with corrosive chemicals. Cathodic protection can se provided by the
sacrificial-anode method. The more cathodic of two metals contacting an electrolyte
causes electrochemical attack of the more anodic metal. Magnesium anodes in
contact with a buried pipeline will be selectively corroded, thus protecting the
pipe. Usually, a small number of anodes, perhaps l-3, are required, and the exact
number depends on soil resistivity. The anodes should be inspected periodically,
as they will completely corrode, leaving the pipeline unprotected after a period
of years. Buried sections of black iron lines should also be electrically insu-
lated from above-ground sections. Inadvertent grounding of the above-ground section
might otherwise override the cathodic protection and accelerate corrosion of the
buried section.
Galvanized pipe is not recommended for gas service because the galvanizing can
flake off inside the pipe and plug the small orifices of crucial gas handling
equipment, such as pressure regulators.
High density polyethylene pipe is often used for underground pipelines by gas
utilities. This pipe has some excellent characteristics, including low frictional
reisstance to flow and good resistance to chemicals. It is usually cheaper both
in material and installation costs, but is somewhat'more susceptible to damage by
careless digging. The pipe is available in a range of pressure ratings up to 1.1
MPa, and is a good substitute for black iron pipe.
The gas recirculation mixer at Monroe was plumbed with CPVCniue which exhibits
favorable high temperature-pressure characteristics. The pipe remains in excel-
lent condition after two years of gas exposure. We exnerienced two gas leaks at
welded fittings in these lines within 9-12 months after installation. This
indicates the need for careful welding technique, if CPVCpipe is used for gas
service.
A gas pipeline will be constructed at Monroe in the fall of 1979 to pipe gas
approximately 1200 feet to the farm creamery where it will fuel a gas-fired boiler.
:”,,I
,‘&l
I '.
The pipeline will consist of nominal 3.18 cm black iron pipe buried approximately
75 cm below ground. Corrosion protection will be provided by bituminous paint,
magnesium anodes, and electrical insulation of above- and below-ground sections.
The pipeline will be equipped with the necessary accessories, and working
pressure will be apnroximatelv 345 kPa. Oneration of this pipeline will provide
useful experience in piping farm-generated biogas.
I
6. Safety
Biogas is no more dangerous than natural gas or propane; however, as with these
other fuels, it should be used with the care due a material that can attain
explosive concentrations in air. The two most important safety precautions are
the avoidance of explosive mixtures of biogas with air and the prevention of sparks.
Since biogas can only explode at concentrations from 9-23% by volume in air, en-
closed areas where gas can accumulate are the most dangerous. Small leaks are
almost impossible to prevent, therefore, good ventilation of enclosed areas is
important. The pungent odor of biogas due to trace amounts of hydrogen sulfide
is an advantage since it makes the nose a good leak detector. The Monroe digester
is equiDped with standard sewage treatment safetv equipment, including flame traps,
pressure relief valves, andan electronic gas detector. The safety equipment has
functioned reliably for two years. The only problem has been occasional freezing
of the pressure relief valve in winter, as mentioned earlier.
Inclusion of numerous shut-off valves in the gas handlingI system provided a con-
venient way to isolate meters, the boiler, and other equipment for removal and
maintenance when required. Isolating with nearby valves allowed removal of equip-
ment without introducing dangerous quantities of air into the gas lines.
In general, the human nose adequately detected a number of small gas leaks that
occurred in the boiler house over the two-year operation of the plant. Soapy
water, which bubbles when applied to a leaky fitting, provided a way to find the
exact location of leaks. Hissing from large leaks could be heard immediately when
the gas was turned on, if fittings did not seal properly during installations.
E. Start-up and Shutdown
1. Overview
Start-up and shutdown of anaerobic digesters can be difficult, time consuming,
costly, and dangerous. Certain wastes do not digest without great care. Severe
weather
. conditions intensify labor requirements, and production outages can re-
quire expensive energy substitutes. Start-ups can be stalled by drugs or other
chemicals in the substrate that may inhibit bacterial growth. Shutdowns are po-
tentially dangerous if care is not taken to prevent explosive mixtures of methane
and oxygen.
Biological stability is reached when gas production begins to rise, and the digester
acids level begins to fall. Either gas flow is monitored or the pH or Total
Volatile Acids (TVA), are measured. If gas production does not rise after a
typical start-up period, the acids level should be monitored daily. The pH
should be rising, the TVA, after peaking, 'should be falling. If this is not hap-
pening, the digester has gone "acid" or tlsourll, meaning the digester must be shut-
dcwn and start-up procedures :,llowed again, but more carefully.
Start-up failures are rare among dairy manure digesters. Normally, either too
rapid loading and acids formation, or harmful chemicals are the cause. Failures
of digesters in general may be due to a lack of seed material or buffering capa-
bility. Seed material containing a rich bacteria culture is used to initiate
digestion in otherwise difficult to digest wastes. Buffering of a digester is
used to minimize the harmful effect of acid formation before methane bacteria are
able to reproduce and consume the acids.
To shutdown a digester, an inert gas such as nitrogen (NJ or carbon dioxide (CO*),
is required to maintain positive pressure and prevent oxygen (02) from entering
the tank while its contents are emptied by gravity or pump. A possible source of
CO2 rich gas is internal combustion engine exhaust. Positive pressure prevents
the tank from possibly imploding by pressure drop as the liquid is removed.
Purging with an inert gas prevents 02 from entering the digester and forming an
explosive mixture with methane.
The Monroe digester was shutdown in August 1979. The shutdown procedure was
unique, in that a second unused digester tank was available to receive the digest-
ing contents of the tank in use. This procedure eliminated the need for another
start-up, since the exceptional biological stability of the substrate allows ef-
fective acclimation to either high or low loading conditions. Ordinarily, with
a single digester, the contents would be removed to fields or a holding lagoon.
The contents were transferred, not because the digester exhibited a loss in
performance or signs of needing repair, but for other reasons. Since the facility
is used to conduct research, the second digester tank was provided with improved
sampling capability. Carefully placed temperature probes were installed to more
accurately determine boiler heating efficiency. Transfer also made it possible
to simplify the loading and effluent piping arrangements for minimal pressure
losses and clogging. Finally, it was also desireable to inspect the digester
after two years of service for.wear and to possibly upgrade its heating system
design.
48
The Monroe shutdown was actually more complicated, due to the transfer circum-
stances. The empty digester was initially purged with N2 to remove the 02. If
enough N2 was available, the tank being emptied could be purged, while gas from
the tank being filled would be vented. To conserve N2, however, the gas lines of
the digesters were connected, and a slightly higher pressure iias maintained in the
digester being filled to prevent backflow of methane into it. Pressure in both
tanks was monitored by manometer connections to independent gas lines. The con-
tent levels in the tanks were first allowed to equalize by gravity after opening
a valve on a pipe that connected them. At this point, the contents of the first
digester were drained to the effluent holding tank and then pumped into the second.
49
IV. BIOLOGICALPERFORMANCE
A. Laboratory Testing
At the beginning of the project, digester contents were tested daily for pH,
acidity, alkalinity, total volatile acids (TVA), percent total solids (%TS),
and percent volatile solids (%VS). Once the system stabilized, the results of
these tests became quite constant, and testing frequency was reduced to twice
a week. Later in the project, acidity tests were discontinued and alkalinity
and TVA were performed only once a week as pH remained relatively unchanged at
7.4. Raw manure influent from the start of the project has been tested daily
for %TSand %VSfor mass balance considerations. Recently, both raw and digested
manure have been tested for chemical oxygen demand (COD) on a bi-weekly basis
to establish typical reduction ratios. All tests were run according to th,s
procedures of standard methods, with a slight modification in testing for total
volatile acids. _
B. System Start-up
Loading of a single digester at Monroe began on August 30, 1977. The digester
was completely loaded over a 5-day period. Manure was scraped into the influent
tank, diluted to 4% TS, and pumped into the digester. The boiler was not in
service until September 15, and the contents remained at ambient temperature
until that time. On September 19, the digester reached 35'C.
Biological monitoring was begun on September 9, 1977 (Figure 21). Total volatile
acids (TVA) was 2000 mg/L, alkalinity was 3300 mg/L, and pH was 6.5. The TVA
peaked at 4000 mg/L on September 26 (alkalinity at 3000 mg/L, and pll still at 6.5).
Since the TVA dropped the next day, daily loading of the digester began on
September 28. The TVA continued to drop to below 1000 mg/L byoctober 2.
50
STAKT UP
b
150
IO0
50
0
230
TO
b-0
Figure 21
Alkalinity and pE also rose to 3600 mg/L and 7.2 respectively by this date.
Carbon dioxide (C02) in the.biogas, consistently above 55% until September 23,
was down to 38% on October 4. Through the month of October, the expected re-
covery pattern continued with a further decrease in TVA and increase in alka-
linity and pH. By November, these parameters had stabilized to those maintained
throughout most of the digester's operation, The TVA stayed below 1000 mg/L,
alkalinity around 10,000 mg/L, and pH near 7.4.
Increases in the loading rate would have continued, but numerous operational
problems associated with winter freezing and flooding were encountered. A
decision was made to hold the loading rate steady until those problems were
resolved. Beginning in 1978, the loading rate was increased to loading all
available manure at 10% TS (averaging 5-6.5 kg VS/m3 a day). Consequently,
retention time has been as low as 12 days, although, it is normally 16 days.
The change in the percent solids loaded required certain influent mixing
modifications, but neither the higher rate or solids level had an adverse
biological impact (Figure 22).
Gas production has gradually improved over the life of the digester primarily
due to increases in production efficiency (Table2 ). Although the digester
stabilized biologically within a 3-month period following start-up, it appears
that in the long term, there developed a more fully acclimated and efficient
bacteria population, independent of operating parameters. Gas production
averaged 178m3 per day over the 23 months of the project including start-up,
freezing and flooding, loading pump overhaul, and shutdown/transfer operations.
Excluding the 5 months when thesecperations occurred, average gas production
was 197 m3/day. During the periodof February through July 1979, it was 226 m3
a day.
,_ _.._
,: -14
52
.-
TABLE 2 Monroe Digester Performance, October 1977 to August 1979
I
l Oct 77. 93 0.170 62 9.4 3.09 3.5
l Nov 107 0,165 75 - 9.1 3.68 5.7 26 0
Dee 147 0,177
____________--------____________^_______-------------- __ 64 10.4 4-72 6.4
__---_--____-------------------
Jan 78 146 0,172 52 9.5 4.85 7.3
Feb 198 0,171 79 12.8 6.63 8.2
Mar 193 0,185 88 11.9 5.99 8.1 24
216
~~~____________,__o~z~s~~~~~~_~~~91,__-,,__-12:1,-_-~:l_l_______ __________------------
8-o
MY 221 0.196 88 12.5 6.51 7.8
Jun 241 0,216 73 12.1 6.45 7.9 25
JOY 201 0.241 58 9.3 4.84 8-2
l Aug 108 0.236 37
------------------------------------------------------------------------------------- 5.4 2.66 7.7
Sep 183 0.208 74 10.0 5.13 7.7
.Oct 144 0.252 68 615 3.35 7.8
28
Nov 145 0,242 92 7-3 3.53 7.2
Dee 154 0,233 90
----------------------------------------------------------------~-------------------- 7.7 3.90 7-3
*Jan 79 108 0.220 85 6, 1 2.90 6.6
Feb 0.220 -. 98 .
206 10.2 5.54 6.7
Mar 0.217 34
234 104 12.2 6.42 6.9
Apr 0 237
_________210-_-_____:-----~---~---~~----------~~~----~:~~--------~:~-----------------
fiY 245 0.233 77 11.1 6.28 7.8
Jun 218 * 0.245 68 911 5.33 8.1
Jly 224 0,193 ' 11.1 9.0 30
70 6.97.
I
l Aug 132 0,238 44 -6-2 3.23 . 7.9
.
‘LOW production during these months was due to:
a) Ott, Nov 77 --the start-up procedure of loading low solids of 4-88 TS.
b] Aug 78;an llday outage of the loading pump for major repairs. r
c). Jan 79--a 15 day period of freezing temperatures and no scraping.
d) Aug 79--a 14 day digester transfer period of no loading.
.
53
.’.:::-‘.-/*.‘z
DIOESl-ER
. .
....:... -..:-. .
....‘r-
- .. .* *.-
.. - -* -.
-. . ‘..,‘.:=.?
.
. .
. - .T
I .
.II .*
I
c
I
. . -.
.
, .
III .
P
‘; ~
-5--zjI?Ix
DEG JAN. FEB.
CJ,v--L
MAR
\ APR. MAY
I
JUNE JULY AU’5
Ph
Gas production efficiency for the first 11 months of operation averaged 0.194 m3
per kg VS added, for the last 12 months, it was 0.228 m3/kg VS added, an 18%
improvement. From April 1979 to the present, excluding July, this figure has
averaged 0.238 m3/kg VS added. In July 19i9, higher solids were loaded up to
12.5% TS, as an experiment to further reduce the digester heat demand and to
document mixing and pumping requirements at higher solids levels. The solids
in the digester rose to 9.0% TS, usually maintained at 8.0% TS. As a result,
the gas production efficiency fell from 0.245 in June to 0.193 in July (m3/kg
VS added). It is not known whether the high solids level in the digester or the
high loading rate of 7.0 kg W/m3 digester volume inhibited gas production
during this month.
The %VSreduced for the first 11 months of operation averaged 25%, while for
the last 12 months it was over 30%. This improvement closely correlates with
the gas production efficiency increase noted above, and is attributed to greater
acclimated bacteria with time.
Influent and effluent samples were analyzed for CODover the period from April
to July 1979. They averaged 82,000 mg/L and 49,000 mg/L, respectively. Average
CODreduction in the digested effiuent was 40% on a voiume basis and 30% on
a weight 'basis.
D. System Shotdown
Transfer of the contents from one digester to the other was made on August 13,
1979. This was done primarily to utilize new and improved monitoring devices
_^__ - 32 --A-.. ,-1--- a-2 “&Gw.,-. r-r2g,
2;; rArdcr.rb n-in; _...I! tn inspect
an
Vii thi, ~cxvu=L u IL;G3 LF;I , t; iiiI,k EGG;:iGac*“r,J
the first digester after two years of operation. Loading of the first digester
ended on August 1, and began again with the second digester on August 16, Heating
of the digester was also discontinued on August 1 to conserve gas for start-up,
and to help keep gas production low.
On August 16, the digester temperature was down to 27'C, and gas production
was approximately 17 m3/day, about 7.5% of normal. TVA remained unchanged,
alkalinity, and pH each dipped slightly, but hardly significantly, throughout
the cool down and transfer procedure (Figure 23). On August 14, they measured
360, 7100, and 7.2, respectively. In addition, recovery of gas production
T
was exceptionally fast. By August 24, it was 212 m3/day, at which point the
biological parameters had already stabilized.
.___~.__..._ ..__
55
.........................
.........................
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........................... l
..........................
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- l
.............................
. l 0 ...........................
l . . . . . :::::::::::::::::::::::::
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. ...........................
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l ’ .........................
........................... .. - l ...
l . .........................
l . m ......................... -. .’
..........................
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l - .........................
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LOAPIM~ RG3-E .........................
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.......................... .........................
l ::::.: .... i’. ... ;“;l::
..
1 I
I ,
.........................
.........................
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... . . . . . . . . . . ............
........................
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TVA ........................
........................
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I
I I I........................
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........................
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ALKALIbJlTY ........................
........................
........................
........................
........................
....................
I I
JUNE. ’ JULY AUGKH-
Figure 23
Digester Performance during System Shutdown
The transfer procedure was similar to two other periods of non-loading and minor
biological stress. The first was for 11 days when the loading pump was out of
service for repairs in late July and early August of 1978. The other was for
15 days during an extreme freeze in-late December and early January of i978/79.
In each case, the bacteria population of the digester exhibited exceptional bio-
logical stability, noted by a rapid recovery upon resumed feeding.
E. Biological Stability
Digestion of dairy manure has presented none of the chronic biological stress
that has plagued municipal digesters. In municipal plants,, the material fed
may differ significantly from day to day, and may contain chemicals which
either inhibit or are lethal to the bacteria required for methane production.
With a farm digester the manure fed does not change dramatically and the addition
of harmful chemicals can be prevented.
This stability makes digestion of farm manures more feasible, since a farmer
need not be concerned with :nonitoring the biological health of the system.
Furthermore, the bacteria demonstrate extreme resistance to stress, especially
in the recovery from periods of non-feeding which is of great benefit should
major repairs and temporary shut-down become necessary. As a result, the lengthy
and involved process of a fresh start-up can be avoided.
57
V. NET ENERGY
A. Overview
The Monroe digester produced a steady supply of fuel gas with 60-65% of the
: heating value of natural gas during 24 months of operation. The gas production
process required energy inputs in the forms of heat and electricity. Gas and
: electric meters measured energy production and inputs to provide data for an
energy evaluation of the system. The net energy is the total gas energy output
minus the energy inputs required to operate the system.
Monthly gas production varied over a wide range during the 24 months of
operation (Table 3). Gas production varied approximately linearly with the
manure loading rate from month to month (Fig. 24).. Thus, variation in loading
rates had a greater effect on gas production than variation in microbiological
efficiency.
During several months when the digester did not receive all the manure from the
180-head herd, and during periods of nonloading, the full potential for gas
producti_on was not realized. The overall gas production rate average was
I
about 178 m3/day given the loading rate reductions. There were two long periods
during which the loading rate was consistent and included all the manure from the
herd, February-June 1978, and February-July 1979. During these periods gas production
averaged 214m3/day and 226m3/day respectively. These figures more accurately
.
represent the gas production potential of the Monroe digester than the overall average.
The gas output of the digester was used to fuel the boiler for digester heating,
run the internal combustion engine for electricity generation, and supply fuel for
heating and cooking in the lab.. These.uses consumed about 47% of the gas;
the remainder was flared. The original plan was to use the net gas output to
fuel a boiler in the farm creamery, however, funds to construct a gas pipeline
to the creamery were not available until the fall of 1979. At this writing,
construction of the pipeline is not yet complete.
C. Energy Inputs
The largest digester energy input was the energy needed to heat and maintain
the digester contents at 35OC. This requirement consumed about 44% of the total
gas production over 23 months. A monthly tabulation of boiler gas consumption is
given in Table 3.
Other energy requirements include electrical energy for digester mixing, and
mixing and pumping the influent. The Monroe digester was designed to be continuously
mixed by a recirculation blower based on experience at sewage treatment plants.
During the first three months of operation, the blower was run continuously,
consuming about 180 KWH/day, which represented 90% of the total electrical demand
of the system. Intermittent mixing was investigated in order to reduce electrical
consumption and equipment wear. Mixing was gradually reduced with no resulting
decrease in gas pr,oduction. From May 1978 through early March 1979, the blower
was operated only during digester loading. Mixing was completely stopped on
March 6, 1979; gas production was not affected over the following six
months. From March through August, the only electrical energy requirement was
the energy needed to mix and load the influent slurry. This requirement averaged
about 20 KWH/day. Electricity consumption is shown graphically in Fig. 25.
The most dramatic improvement in net energy was the elimination of blower use
resulting in.a 90% electricity demand reduction. During the first five months
of digester operation, net energy was also improved by increasing the solids
in the influent loaded from 4% to 10% TS. Since the volume loaded remained
roughly the same, in effect this change represents an increase in the quantity
of solid material loaded. With heat demand held constant, this improved the
net energy by enhancing gas production.
Later in the project, an increase from 10% to 12% TS was made with no increase
in the quantity of solids loaded but with a reduction in the amount of water
added. This procedure resulted in a reduced digester heat demand and a small
increase in retention time. The improvement in net energy, however, was unable
to be quantified due to constantly changing ambient and operating conditions.
Net energy for the 23 months of digester operation is shown in Fig. 26. Low
loading rates from August 1978 through January 1979 with resulting low gas
production affected net energy results for those months. Net energy yield
was about 56% for the best digester performance period, February 1979-July 1979.
For the twelve months including the best performance period, August 1978-July
JY
TABLE 3 GASPRODUCTION
AND BOILER CONSUMPTION
T""_________----_~~~------------~~~~------------~~------~.------------~~~---------
Sept . 183 5.13 74 40
*act 144 3.35 68 47
*Nov 145 3.53 92 63
*Dee 154 3.90 90 . 58
-------------------------------------------------------------~-------------------- .
*Jan 79 108 2.90 85 79
Feb 206 5.54 98 48
Mar LJ
, .4' 6.42 104. 94
APr 230 5.79 80 35
-----------------------------------------------------------------------------------
May 245 6.28 77 31
June 218 5.33 68 31
July 224 6.97 70 31
*Aug 132 3.23 44 33
--pcI-... -.. -
F
--__
3Y' --
GAS PRODUCTION
AND BOILER CONSUMPTION
I""----__---____-~"I------------~~~~------------~~------.-------------~~---------
Sept . 183 5.13 74 40
*act 144 3.35 68 47
l Nov 145 3.53 92 63
19sf_--_-----_____f'~--------.----~~~~------------~~----.-------~-------~~----------.
*Jan 79 108 2.90 85 79
Feb 206 5.54 98 48
Mar I4.3.4' 6.42 104. 94
APT 230 5.79 80 35
-----------------------------------------------------------------------------------
May 245 6.28 77 31
June 218 5.33 68 31
July 224 6.97 70 31
t"4_______-----__'ff------------~:~~------------~~-------------------~~-----------
*Low production during these months was due to:
a) Ott, Nov..77--the start-up procedure of loading low solids of 4-8% TS.
b) Aug 78--an ll-day outage of the loading pump for major repairs.
c) Ott-Dee 78--low loading rates resulting from incomplete scraping.
d) Jan 79--a 15-day period of freezing temperatures and no scraping.
e) Aug 79--a 14-day digester transfer period of no loading.
“.’ --‘P -
Y= atc+b
3 4 5 6 i
uwAN6 RATE
. ( Kg~+y~ay)
Figure 24 - Relationship,of Gas Production Fr Loading Rate
rdJMMJ5NJAMJ
1977 ‘76 ‘73
/4K’N-I-H 5
---- ..-
........................................................... ...........~....~~.~.........~..~.~~......~...............
..~~..................................... ...........................
................................................
................ .........................................................
........................................... ................ ...........................
..........................................................................
........................................................ .............................................................
................................................................................. :
..............................
................................ ..--....................:::::::~:~:::::::~:::::::::::::::::::::!~:.:.!:::::::::::
.......................................
............... ........................I.............~~~:::
:,~~~~.~~~~~~r”~~:~~
.......................... ............................................ ..,....: ...................
................................................. ..~-.
.‘. ‘,
62
1979, net energy yielded about 51%. Since these months included the six months
of low loading rates, an estimate of the annual potential net energy of the
Monroe system is probably close’to the best six months performance, 56% of the
gross gas production.
The Monroe system is not yet at optimum net energy as opportunities for energy
savings still exist. The most promising is improving the efficiency of the
heat delivery system. It was observed during the winter of 1978-1979 that the
boiler consumes excessive quantities of gas, up to 10% of daily gas production,
just to keep itself up to temperature in cold weather. Installation of a flue
damper valve has potential to save a significant portion of this gas.
-- -
VI. ECONOMICS
While assessing the economics of anaerobic digestion technolD.gy sized for farm
scale operations and resources, the economic analysis has some special require-
ments and problems. The methodologies used for evaluating energy producing
technologies are often adapted from traditional analysis conducted by utilities.
or private energy conglomerates to evaluate alternatives for central energy pro-
. duction. -This Style Of analysis is not as applicable to small-scale decentralized
-technologies such as a?acrohic Jigesticn. There p-p’? $~=l.rpYq~??
_iVrnnrtaitt
.__._ ~.~~-ppJies:
.
1) The consumer of energy produced by anaerobic digestion is also
the producer. The financing methods and acceptable rates of return
are very different for a farmer or consumer than a utility.
2) The utility assumes that a single economies of scale curve
can be drawn for a given technology (e.g., a thermal power plant).
For anaerobic digestion, a series of.curves would be available
depending on the design trade-offs, farm size operation, and the
sophistication of the existing manure handling system.
3) The farmer will experience a rising cost of competitive
energy (electricity, natural gas, oil). Since these are rising
much faster than inflation, the investment decision and, indeed,
the long-term rate of return on the investment capital will be
strongly influenced by the rate of energy cost increase.
4) The farmer is faced with rapid inflation in all costs. The
value of any capital investment will increase over time. Even
if energy costs rise at the rate of inflation, a capital investment
that produces a benefit will ultimately be a good investment as
the value of money falls.
5) Anaerobic digestion has other non-quantifiable benefits such
as pollution control, odor control, increased ease in manure
64
For-this report, an economic model has been developed and used that overcomes many
of the difficulties of present inappropriate economic methodologies for evaluating
farm scale anaerobic digestion. The economic model uses standard life cycle cost
formulas for computing the price of energy necessary to cover all associated
lcosts (See Appendix 2). The analysis balances the capital costs, the
operating and maintenance costs, tax benefits, interest rates, and fuel escalation
costs against the energy produced over the life of the facility. It also includes
options for both owner financing and utility financing.
This economic model provides the flexibility to examine the impact to varying _
parameters such as financing options, capital costs, inflation rates, interest
rates, and capital credits. Thiq flexibility allows an evaluation of how to
optimize the economic return from a system, as well as comparing the cost of
energy produced from this technology to the cost of energy from other technologies.
In the analysis, two financing options are examined. Cne system is financed by
_._. .. -
a farmer, and the other is financed by a utility. as part of its new electrical
generating capacity. .Within each of these financing options, both digestion
systems that include manure handling components and those that are an exaansion of
existing manure handling systems, are examined. Any system can be evaluated for
producing gas or producing electricity. This effects a system's capital cost,
maintenance costs and operating costs. Most options are examined at both two
hundred and four hundred head dairies. Because of the difficulty of assigning
a cost of labor to a farm operation that does not require hiring a full-time
operator, the economic information is presented for both a labor cost of $4.00
per hour, raised with the rate of inflation, and for no labor costs. One additional
system is evaluated for an owner-built system at the ZOO-head size. All options
are evaluated with no credits taken for other benefits, and assuming all the
energy produced is used. The other assumptions common to all options are presented
in Table -4.
Table 4.: Life Cycle Assumptions
1. Inflation 10%
2. Fuel Escalation 13% f
3. Interest/Opportunities Cost 12% .
4. Life 20 years
5. Credits on Capital 20% Investment Tax Credit
$3,500 Clean Water Act Credit
(for farmer financed systems that
include manure handling)
6. Tax Rate (marginal) 0.2
7. Competitive Energy Costs $3.69/GigaJoule
$O.O4/kwH
8. Efficiency of electricity
Production 20%
For a farmer financed system, the interest rate on the capital investment is
assumed to be 12%. The annual payment is computed by standard mortgage interest
formulas. For the utility financed system, a different method is used. Utilities
allow two sorts of capital costs, the first being a rate of return or profit on
their invested capital (equity), and the second, cost of the capital borrowed (debt).
The output and cost assumptions that vary in different options are listed in
Table 2;' These include energy production, capital costs, and op.erating and-ma&
tenance costs. The capital costs vary for the following reasons. If a system
produces gas as the primary output, no engine generator is required. If electri-
city is the primary output, the need for a boiler is eliminated. If manure handl-
ing is not included, the costs of the manurehandling pump, the influent tank,
and the manure handling plumbing is eliminated, and the labor costs are reduced
to reflect only digester operating labor, as distinct from manure handling. For
the site-built system, the labor construction costs are reduced and the profit
for the company providing the packaged system is eliminated. Maintenance costs
reflect need to completely replace each piece of equipment once during the ZO-year
life, and to account for the inflation that would occur in the costs over 20 years.
Y..
Table 5 : Energy Outputs, Capital, Operation and Maintenance Costs for Various
Digestion Systems
NOTE: output, operator cost, and maintenance cost are on an annual basis.
The cost of energy produced by the various systems is presented in Tables 6 and L.
All owner financed systems produce energy that is less than the present cost of
propane or fuel oil. Systems that discount labor are less than or equal to the
cost of natural gas in many areas of the country. Figure 27 compares costs of various
fuels available to farmers with costs of bio-gas produced from anaerobic digesters
and-ffsynthetic fuels."
This suggests that perhaps a farmer-owned digester producing energy is the most
cost effective overall. Certainly, the farmer is given the opportunity to profit
over the utility. If the farmer insists on a rate of return similar to the
utility, then very likely the "cost" of the energy leaving the farm would be
similar. The energy costs in Table -7 do not include this profit, but rather
provide the "break even" cost for the farmer. Since the farmer also accrues
benefits other than energy, a "break even" selling price is Feasonable since that .-.. _
price pays for all costs, thus the remaining benefits are free.
The analysis takes into account current incentives available for this type of
investment. The impact of these incentives, however, is not great.
Recent federal legislation has been proposed that would provide low interest loans
to finance the purchase of solar technologies., Some versions of the legislations
provide interest subsidies of up to 6% less than the current interest rates. To
assess the impact of this financial incentive on the economics of digestion, a
200-head packaged system was evaluated at a range of interest rates from 6% to
12% [Figure 28). The impact of this sort or‘ incentive program over simple capital
or tax credits is considerable.
.
200 Head Systems
Table 7 : Cost of Electricity for Farm Scale Digestion Systems . in $ per Kilowatt Hour
c
\‘
:;\’
.. .
l3l-2
00
I
0 0
Figure 28
is, however, not the only criteria by. which an energy source should be judged.
This analysis demonstrates that the energy produced by anaerobic digestion is
competitive with present energy costs and with the utility's marginal cost of
1 production. With any decentralized technology, this should be the primary cri-
teria for evaluation, not its overall impact, for there are many technologies
that produce only a small percentage of our national energy needs at competitive
costs. Individually, the technologies are of little consequence, but collectively
they form the basis for a national energy independence that is within our means.
Anaerobic digestion can make our dairies and feedlots'significantly less dependent
on fossil fuels and net energy producers. This would be an important step in the
development of an agriculture that is increasingly less vulnerable to the uncer-
tainties of our current energy supply and to the devastating inflation rate
associated with that supply.
72
APPENDIXI
Calculation of the Slurry--. ride Film Coefficient of the Draft Tube Heat
? k-14 4 Dl + 30 in.
A= 45.4 ft'
C. Overall heat transfer coefficient
U,= Q Where LIT = 22.8'F
AOm Q = 1965 Btu/min
A = 45.4 ft2
“0
= 114 Btu/hr-ft2-F = 2.33 x106 joules/hr-m O2- 0C
_5
c. Calculate the water-s ide coefficient
= 0.023 (Re)0*8Pr0.33 Where Re = 66778
hiDH
k Pr = 4.05
= 0.33 ft
DH
k= 0.372 Btu/hr-ft-OF
h. = 296 Btu/hr-ft2-0 F = 6.05 x lo6 joules&r-m2 - 'C
1
might meet the need for fuel. This is flawd reasoning. for
e consumer investment decision is not bared on the rate of
return, paybSck period, or life cycle economics of that
The basis of solar economics is discussed in the context of particular investment. In fact, few if my consumer
four technologies. Passive/hybrid solar heating in new and investments arc based on such long-tern considerations. The
remodel Spplicrtioa. Solar hot ‘mter heating. active solar initiS1 cost has dominated consumer decisions, and at best
hating, and enaerobic digestion rre compared on payback a vague knowledge of the life-cycle performance is included.
priods. rate of return, and the cost of energy generated/
saved by these technologies. A life cycle Smlysis will Nevertheless. the use of this analysis is instructive in
foa the basis of the comparison, which includes operating dealing with design decisions for specific clients, and
dam as the basis for the life cycle ersumptions. The in providing a consumer-oriented picture of a systems
capital costs. operation costs. and maintenance costs will economics to rhc consumer. This should not be contrasted
be considered. Ss well as fuel escalation and inflation. with the value of the solar sysrca in its larger economic
and social context. The important concepts here center on
The output from this analysis will be compSrcd to the the interrelationship between capital costs rnnuallred over
present end future marginal cost of energy produced from the life of the investment. and annual fuel costs for the
‘conventionrl ’ energy sotwccs such as oil and electricity. energy Source being replaced. These cost strews arc
. and Sn evaluation of cost of the various energy production edified by three important factors: interest or discount
options including solar-bared renewable technologies will rates. inflation rates, and fuel cost escalation rates.
be included. Given that these are constant over the life of the
. investment, and thnt the fuel escalation rate is larger
tnan the inflation rate. ea curves can be dram (ICC Fig.
SIBFURY 11. In this cese capitS costs Sre l ssumrd to be
annurlized by S mortgage payment formulS:
The dcvclopment of solar energy es a viable energy
i
producing technology has progressed considerably in the AP-cc ( 1 (1)
OolsWR ECONOWICS
75
-N
J l*c i I- (I**)
ln I.\;) ln tI,r’CC (I- [**iI-IV) ( ln 11.~) ) l II
K-
(6)
.
76
CONSS4Hi IJTILln
mum conscrva~ion 1300 91 4% 910 3.6 -11 130 .91 130 .ss
,ivc solar * 5200 73 365 730 11.4 .06 1240 3.02 520 5.28
Ye molar 11200 76 380 760 15.1 .OS 1840 4.60 820 7.95
,crvrtion/ 6500 107 53s 1070 10.4 .Ob 1370 2.77 650 4.61
msivc solar
,trvrtion/ 9500 110 550 1100 13.3 .OS 1970 3.79 950 b. 3ll
ire solar
mm conservation 1900 74 370 74” 5.5 .I0 190 1.55 190 2.33
due solar 3000 45 225 450 10.2 -06 750 3.76 300 6.52
IL solar 5900 45 225 480 lb.1 -02 1390 7.09 590 12.39
8rrvationf 4 900 92 400 920 9.1 -07 940 3.09 490 5.07
,sive solar
.errationf 7800 95 495 990 12.2 .M lS80 4.57 780 7.69
ire solar
a4300 2833 8499 28330 9.3 .06 14130 2.94 8430 3.26
69400 ii24 4272 14240 13.1 .w 12640 4.62 6940 6.20
60700 b07 2061 6870 18.7 -00 11770 1.01 6070 10.90
consumer invertmcncs analysis uses those credits fits accruing to the whole society char arc not necessarily
lablc to a consuacr such 81 she solar tar. credits, attractive to an individual. For this reason the utility
c the utility rnrlysis uses only the 10% invcstxcnt tax a.?d its economic benefits must be considered as a viable
‘its. The cost of energy to the consumer is based an a opt ion.
CJCJC cost. rich no residual value at the conplerion of
invesrmcnr’s economic life. This is probably nor true. In Care III the anaerobic digester comparisons illustrate
cially in the case of a new house with a passive system. the cconoaies of scale associated with this technology.
syrrs could be expected to last (and )avc energy) for Here when compared to current gas costs, economic scale
~ng as the house, which should be at lust twice as long might bc about 200 cors;~hcn conparcd to m.arg~nal costs
he 'economic life’ of the mortgage. men 8 very small digester of this type wuld be
economically feasible at the margin.
utility economics presented also assume no residual I
c; korcrcr. this is less severe in that the utility may
rked to turo its invcsrmcnt over to the borrower after it fable 7. MSIJWTIONS FOR LIFE CYCLE ANALYSIS
received its rate of return for the ‘economic life.’
c 3 provides the relevant cost comparison for utility Interest race 121
meing. Avsrngc rate of return (utility) 12\
Inflation 78
cncral. with addition of fax credits for solar and Fuel escalation costs 1u
crvation investments, the pryhck periods and rate of Credits (home owner)
m become quite attractive, euen for relatively expensive insolrtion credit .1a
HI,. The cost of a passive solar option for a new house rcncw=ble credit 5M first 52000,
-f $2.77/MElLls saved, ataut 60% of the current cost of 2m next $8000
I,’ to the consumer. This of course ignores other Credits (ctiliry)
Bmic benefits and the increase in the home’s long-term invcsmcnt credit 10%
CL v8lue. Tu r8tCs
homeowners 2a
re solar systems are somewhat lore expensive, but with utility 48%
its they remain an attractive investment when compared Life
mp-trm energy costs. Both active and passive systems new construction 30 yurs
combined in 4 toral energy package for a home yield remodel 20 yems
.cffccrire energy ravings, with payback periods methane digester 25 yews
untially below the life of chc mortgage. However * Residual value SO
c most homeowners mve within sir y~rs. the feasibility
ast of these options depends oo the increase on thm sale
I of the home or some further subsidy to make this
-effrzrirc invcsucnt also artractivc to the avorago
wtx.r. This suggests rhrc sine the cpcrgy saving bene-
77
ENRGY FOR ENERGY PRODlXTlDN TF: total savings over the economic lift
It: payback year
n the life cycle costs of solar cncrgy are compared on an c: total cost of operatlon, the investment over the life
ividrvl basis. the economics are attractive. The issue. )I: rake of return to the consumer
ever, Is LDI solar energy ss @ consumer invesrment. but E: rota1 energy produced/savrd over tht ecor&ic life
economic standing when compared with the alternate (llnJs, Khli, etc.)
s to acquire the next units of energy. The cost of COE : average cost of the produced/saval energy over the
se units is known~urginal cost. economic lift of the investment
l-Z.50 2.50
S-7.50 7.50
8-12.00 12.00
s-10.50 10.50
gobic Di;estion
Do COYS 3.20
00 COYS 6.20
10.9a
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