Failure Investigation Enhances Reliability of Machinery
Failure Investigation Enhances Reliability of Machinery
Goodwin
Practical Failure
Failure Analysis
Analysis Volume
Volume 3(2) April 2003 21
Thorough Failure Investigation in Enhancing the Reliability of Machinery (continued)
sailing up the shipping channel off the When the failed hoses were exam- report,[6] which was published just a
port of Fremantle, one of the hoses ined after the event, there was clear few weeks before the accident to
failed, causing a substantial leak of evidence of high-cycle fatigue failure. HMAS Westralia, that pulses with
fuel oil. The engine was shut down, The two burst hoses had failed in pressures at least an order of mag-
but a few minutes later a second hose fatigue, and further inspection reveal- nitude greater than the static pressure
failed, this time on the other engine. ed broken wires in the steel braiding were emitted by injection pumps,
Before the second engine was shut of several of the hoses. Some of the and that the phenomenon was not
down, leaving the ship without unfailed hoses from the engine were widely understood when this engine
propulsion, a fierce fire broke out. also tested to destruction and failed modification was made in 1998.
Tragically, four young sailors perished at a wide range of pressures. One with
in the engine room fire, and the vessel over 50 broken wires failed at 6000
came close to running aground before kPa. Figure 4 is a close-up of the
a tow was able to be secured. braiding showing the way the wires
were laid up. (Crossed wires such as
The accident, investigated by a
those seen in the center of the image
Board of Inquiry, was found to be a
were found in a number of places and
direct result of the modifications to
were judged not to be a significant
the low-pressure fuel system using
problem.) The individual wires are 0.3
flexible hose. This was intended to
mm in diameter. Figure 5 shows a
simplify a problematical maintenance
micrograph of the end of a wire from
activity, and, on the face of it, appeared
one of the failed hoses. Close inspec- Fig. 3 The failed hose found to be responsible
logical. A photograph of the failed for the engine room fire on HMAS
tion of the fracture surface revealed
hose appears as Fig. 3, which is re- Westralia in 1998
the characteristic progression marks
produced from the report of the Board
of a high-cycle fatigue failure, and the
of Inquiry.[5]
lack of necking also pointed to a fati-
The initial investigation centered gue failure. By contrast, when a new
on a mechanical and metallurgical hose was tested to destruction, the
study of a burst hose that had been broken wires were examined micro-
found to leak fuel onto a hot spot, scopically and found to be severely
leading to a serious fire. The main necked before failure. The report of
reinforcing material of the hose, a this work[9] was tendered in evidence
hard drawn type 304 stainless steel to the Board of Inquiry.
wire, was found to conform to the Fig. 4 Close-up of braiding of reinforcing
specified standard, as given in BS It was concluded by the Board of
wire around the type of hose shown in
1554:1990, both for chemical analysis Inquiry that the system was subject Fig. 3
and hardness. The hose supplied had to pulsations that had not been under-
a specified minimum burst pressure stood when the engine modification
of 33,000 kPa. Some spare unused was made. Calculation showed that it
hoses were tested to destruction and would take approximately 66 h for
failed at pressures in excess of 40,000 each injection pump to produce one
kPa, significantly higher than their million spill pulses. The first failure
rated strength. The static pressure in occurred after approximately 50 h.
the system was approximately 600 Assuming each hose was affected only
kPa, so it was clear that the hoses were by the pump to which it was attached,
rated to over 50 times the static pres- this places the number of stress cycles
sure in the system and were actually in the hose at the lower end of the
Fig. 5 Micrograph of a broken wire from a
stronger than their rated burst pres- regime known as high-cycle fatigue. It braided hose of the type shown in Fig.
sure. So why did they fail? was clear from the MSA research 3, with progression marks
initiation site. A diagram of the design was modified to mount them ces due to the flow and the motion of
arrangement is shown in Fig. 9. on the bedplate. A downpipe ap- the pipe. This was also exciting other
proximately 1.5 m long was inter- vibration modes in the pipes. Such
Pulsation dampers (lower left of
posed between the rails and dampers. vibration imposed an unexpected
Fig. 9) were fitted to each fuel rail to
An unforeseen result was that the strength requirement for the joint,
mitigate the pulsating flow that was
oscillating mass flow now had a verti- which simply could not be met. While
causing vibration elsewhere in the
cal component in the downpipes. it has been possible to stiffen the
system. The mass of fluid in the off-
These were relatively poorly re- pipework to reduce the failure rate, it
engine pipe system was such that
strained in the vertical direction, most is clear that mitigation of the
considerable pressure pulses were re-
of the restraint being supplied by the pulsating flow closer to the source
corded. The original plan was to fit
flanged coupling at the damper. Fig- would provide a more satisfactory
the pulsation dampers directly to the
ure 10 shows the welded coupling solution. The solution proposed by
end of the fuel rails, to isolate pul-
used to join the pipe to the damper. DSTO is still in the course of devel-
sating flow along the rails from the
The design was obviously never in- opment, but the addition of smaller
off-engine pipework.
tended to cope with large bending accumulators directly to the fuel rails
The pulsation damper is essentially loads and failed adjacent to the weld. is showing promise.
a hydraulic accumulator, with its Figure 11 shows a cross section of the In all the cases cited, the failure
connecting manifold configured to failed joint, with a clean straight crack mechanism was clearly metal fatigue.
prevent pulses bypassing the accumu- through the pipe outside the weld. However, the diagnosis of the cause
lator. Adding this device would trans- The initiation site in this case appears of failure led to the identification of a
mit much smaller pressure fluc- to have been in the heat-affected zone design issue in the injection pumps.
tuations into the rest of the system but at the toe of the weld, though the exact Fatigue failures, especially in fluid
give rise to increased oscillating mass location is of little importance in this systems, are sometimes initially iden-
flow along the rails, which were case. The quality of the materials and tified as the result of material inade-
well restrained in the longitudinal work was not in doubt here. Any stress quacies, while a wider study of these
direction. concentration at the toe was small. systems revealed that a design change
When the installation was made, it The problem arose because of the in the fluid process could substantially
was found that the specified pulsation rearrangement of the design of the reduce cyclic loads.
dampers were too big and heavy to fit pipework during the refit.
directly to the end of the rails, so the A Diesel Engine Auxiliary
Measurement of the vibration and
Gearbox Failure
of pressure at the flanged connection
Marine diesel engines have numer-
to the damper[12] showed a close cor-
ous auxiliary machines and devices,
respondence between the inertial for-
cracking in the repair procedure. to be a major contributor to a failure, as early as possible and in as undis-
Experience so far is encouraging, and especially in welded structures where turbed a state as possible. If a mech-
no new problems have emerged dur- defects are almost inevitable and in anical engineer and a metallurgist (or
ing the first few years back in service. some materials very difficult to detect. other materials expert where non-
A realistic designer uses a factor of metallic materials are involved)
In this case, a comprehensive failure
safety sufficient to allow a credible examine the site together, the differ-
analysis was neither practicable nor
defect (one that might reasonably be ent perspectives are synergistic. In the
regarded as necessary. The main
expected to occur and not be detect- experience of the author, the mech-
loading mechanism, while difficult to
ed) to not lead to a failure under the anical engineer typically looks out-
quantify, was easy to identify. The
anticipated loading. ward, for the source of loading or
upgrades to the engine could be
When a failure has occurred, and foreign bodies, while the materials
shown not to increase the camshaft
particularly when other similar scientist tends to look inward, seeking
loads significantly. Therefore, it was
failures have occurred or a safety- clues in more microscopic details. An
possible to show with confidence that
critical component has failed, the experienced investigator may cover all
a small increase in effective strength
investigator needs to determine such aspects, but it is unusual to find
was sufficient to produce a repair with
whether or not the loading exceeded an investigator with a sufficiently wide
a life at least as long as that of the
that expected by the designer. It can range of skills to do such a job alone.
original joint and with a reasonable
be very difficult to revisit the original One expert might home in on a
prospect of increased life.
design decisions, especially in mach- particular theory and eventually
propose a sequence of events and
Reflections inery whose design has evolved. The
causal factors not supported by all the
In many of these cases, the investi- component designer is not likely to
be available for consultation, and the evidence. A team is more likely to
gation began with a single failed question theories critically. In the end,
component being forwarded in a crate design may have been based on “pencil
and paper” methods that are not the explanation must be supported by
to the laboratory with a request for a all the evidence.
metallurgical investigation. The user amenable to reexamination using
wants to know why the item has failed. modern methods.
In engine work, and in many other
Provided fracture surfaces have not After a failure, it is important to machinery applications, there is a
been too seriously damaged, the determine the sequence of events that tendency for the machine to do much
metallurgical investigation is likely to led up to the failure. Once the first damage to some components in the
reveal whether or not the failure is a component to fail has been identified, vicinity of the failure during the time
sudden overload or fatigue and may the best way to determine the loading in which the machine is shut down
identify stress corrosion or other may be for the investigating team to and comes to rest. Sometimes the
failure modes. It may sometimes find assess the loads independently of the original evidence of the failure is
a material defect at the initiation point manufacturer, then compare the two actually destroyed, and it is then a
of the fracture. Such a defect may not calculations if possible. In this way, difficult job to make any reliable
be the prime cause of the failure; a different assumptions made by each determination of the cause of failure.
normally acceptable defect may party may be brought to light and Many components may be damaged,
simply have provided a starting point their validity challenged. In this and it may not be at all obvious which
for a fracture, driven by a load the process, ideally both the design as- failure occurred first. Furthermore,
designer did not anticipate or by sumptions and the assumptions of the failures sometimes lead to damage to
vibration causing a cyclic component investigators can be tested before surrounding items, such as local fire
of load that was not expected. conclusions and repair or modifi- damage, and so forth. In such situa-
The specified strength of any cation options are finalized. tions, the introduction of physicists
material includes consideration of Where a failure occurs to a major and chemists into the team to explain
assumptions and statistics about the piece of capital equipment, it is ad- the condition of some of the wreckage
size and frequency of defects. Some- vantageous to have as many informed can be invaluable. Coming from a
times a defect can genuinely be said eyes as possible examine the wreckage multi-disciplinary Defence laboratory,
by Herman Research Laboratory on sional Engineering Publishing Ltd., Lon- Pty Ltd, Welshpool WA, Report 8H24/
behalf of the ship owner. The quality don, 2002, p. 13. M1, June 1998.
of the work of these laboratories, and 2. W. Wong: How Did That Happen?– 10. Departmental Investigation into the Engine
where appropriate the permission of Engineering Safety and Reliability, Profes- Room Fire on Board the Australian Antarctic
sional Engineering Publishing Ltd., Lon- Research and Supply Vessel AURORA
the owners to use these images, is duly don, 2002, p. 128. AUSTRALIS at the Antarctic Ice Edge on
acknowledged. Figure 15 is from an 22 July 1998, Incidents at Sea Report 135,
internal DSTO report and was 3. D Woodyard: Pounder’s Marine Diesel
Marine Incident Investigation Unit,
Engines, 7th ed., Butterworth Heinemann,
generated from the excellent FEA 1998, p. 158ff.
Commonwealth Department of Transport
modeling work of Hai Hoang Tran, and Regional Services, Canberra, June
4. M. Jennings: Prevent the Leak; Cut the 1999.
formerly of DSTO’s Maritime Risks, Marine Engineers Review, Sept
Platforms Division. 1998, pp. 13-15. 11. G. Goodwin: Report on the Failure of a
Flexible Hose in the Engine Room of RSV
DSTO staff who have made a 5. Report of the Board of Inquiry into the Fire Aurora Australis, Leading to the Fire of 22
particular contribution to the investi- in HMAS WESTRALIA on 5 May 1998, July 1998, published as an Attachment to
Defence Publishing Services, Canberra, Ref 10.
gations described in this article 1998.
include Dr. Stan Lynch, Dr. Len 12. S. Teo: Vibration and Pressure Pulsation
6. J.R. Galpin and M.E. Davies: Failures of Measurements on Main Engines Fuel Lines
Davidson, Dr. Darren Edwards, Dr.
Low Pressure Fuel Systems on Ships’ Diesel on the HMAS Westralia, AMEC report
Bob Phillips, Stewart Alkemade, Engines, BMT Edon Liddiard Vince Ltd., prepared for Defence Materiel Organi-
Alban Cole, Max Bentley, and Tom MSA Research Project 401, Marine sation, July 2001.
Fraser. A number of invaluable lessons Safety Agency, Southampton, Jan 1997.
13. R Phillips: Weld Repair Procedure for
were learned from interaction with 7. J. Cannell: HMAS Westralia Fire 5/5/98, Camshaft Bearings in ALCO 251C Engines
them. Without the diverse skills and Study of Fuel System Characteristics, Final in RAN Service in LPA Vessels, DSTO
insights brought to the work by these Report, Engineering Dynamics Pty. Ltd., report to LPA Project Director, 1998.
unpublished report for Director of Naval DSTO File No. 495/206/0257.
people and other colleagues, the con- Materiel Certification, Canberra, 12 July
clusions of several investigations 2000.
would not have been reached as
8. H.J. Gatjens and H. Rulfs: Damping of
quickly or reliably, and in some cases Pressure Vibrations in Fuel Systems of Ship
the author’s initial theories might not Diesel Engines, Hansa, Sept 1990, 127(17/
G. Goodwin, Senior Research
have been debunked as promptly. 18), p. 1064ff. Engineer, Marine Propulsion, DSTO
Maritime Platforms Division, Cordite
9. J. Bromley: Metallurgical Examination and
References Testing of Flexible Fuel Hoses, Report for
Avenue, Maribyrnong, Victoria, 3032,
1. W. Wong: How Did That Happen?– the HMAS WESTRALIA Board of Australia. Contact e-mail: geoff.
Engineering Safety and Reliability, Profes- Inquiry by Metlabs, AMEC Engineering [email protected].