Leak Sealing Procedure
Leak Sealing Procedure
EPRI
Electric Power
Temporary Repair
Leak Sealing
Sealant Extrusion
Project 1328-1
Final Report
May 1983
Research Institute Sealant Chemistry
Mechanical Sealing
EPRI-NP—3111
DEBS 902677
Prepared by
Combustion Engineering, Inc.
Windsor, Connecticut
DISCLAIMER
D IS C L A IM E R
N P-3111
Research Project 1328-1
Prepared by
Principal Investigator
G. A. Smith
Project Manager
N. R. Stolzenberg
Prepared for
NOTICE
This report was prepared by the organization(s) named below as an account of work sponsored by the Electric
Power Research Institute, Inc. (EPRI). Neither EPRI, members of EPRI, the organization(s) named below, nor any
person acting on behalf of any of them: (a) makes any warranty, express or implied, with respect to the use of
any information, apparatus, method, or process disclosed in this report or that such use may not infringe private
ly owned rights; or (b) assumes any liabilities with respect to the use of, or for damages resulting from the use
of, any information, apparatus, method, or process disclosed in this report,
Prepared by
Combustion Engineering, Inc.
Windsor; Connecticut
EPRI PERSPECTIVE
PROJECT DESCRIPTION
Temporary on-line leak sealing of components (such as valves, flanges, and pipes)
that is performed while the system remains in operation may provide the plant oper
ator with an alternate to an unscheduled plant shutdown to effect a permanent
repair. This temporary repair may be cost effective in avoiding the loss of revenue
resulting from the shutdown and additionally may prevent damage to the component
(due to steam cutting, etc), which requires extensive and costly maintenance to
achieve a permanent repair.
This project (RP1328-1) evaluates the effectiveness of commercial leak repair ser
vices, with particular emphasis in the application of the on-1ine sealing techniques
in nuclear power plants. No attempt is made to determine if one vendor, furnishing
this leak repair service, is superior to another. The work performed in the project
is intended to provide guidelines to assist utilities in making the decision on
whether to apply this on-line leak sealing method and what to expect if the decision
is made to apply it.
PROJECT OBJECTIVES
The objectives of this project are to determine the limitations of the use of on
line sealants to temporarily eliminate leaks in process systems in nuclear power
plants and to provide conclusions and recommendations on the use of these materials
and techniques.
PROJECT RESULTS
Three companies, which provide on-line leak sealing services, participated in the
project by demonstrating their equipment and techniques used in sealing a variety of
leaks. A fourth company participated in a limited part of the total test program.
The leak repair equipment and techniques used were commercially available at the
iii
time the tests were conducted (August 1980 to January 1982). The participation of
the following companies in this project is gratefully acknowledged:
The above order of participants does not necessarily correspond with the identifica
tion of Vendors A, B, C, and D shown in the text of the report. No single organiza
tion was clearly superior to the others.
Performance results indicate that leak sealing of valves was generally less success
ful than leak sealing of pipes and pipe flanges. A number of recommendations were
developed as a result of the work performed. Utilities contemplating the use of an
on-line leak sealant service should consider, in detail, each of the recommendations
noted in this report and should work closely with the organization that will perform
the service.
Each of the above listed participants was given the opportunity to review and to
comment on this report. One of the participants provided a 1ist of items that
should be evaluated by potential users of on-line leak sealing services and re
quested that the 1ist be included as an addendum to the report. This, however, was
not incorporated because the list generally parallels the conclusions and recommen
dations of the report. Briefly summarized, potential users are encouraged to com
prehensively evaluate leak repair services in areas such as, but not 1imited to, the
following:
iv
T. W. Libs and R. E. Swanson. However, questions on the content of this report
should be directed to B. P. Brooks.
v
ABSTRACT
specimens were left on-line at pressure and temperature with thermal and
pressure cycling for as long as 14 weeks to determine longer-term repair
durability. Sealant samples were thermally aged, irradiated, and analyzed
for the presence of reactive components such as sulfur, heavy metals and
halogens.
vi i
CONTENTS
Section Page
1 INTRODUCTION 1-1
2 OBJECTIVES 2-1
Vendor A 4-1
Vendor B 4-2
Vendor C 4-3
Vendor A 5-1
Vendor B 5-3
Vendor C 5-4
ix
CONTENTS (continued)
Section Page
Vendor A 6-2
Vendor B 6-3
Vendor C 6-4
Vendor A 7-1
Vendor B 7-2
Vendor D 7-3
Conclusions 8-1
Recommendations 8-3
9 REFERENCES 9-1
x
ILLUSTRATIONS
Figure JLeIS.6
Figure Page
xi i
TABLES
Table Page
xi i i
SUMMARY
S-l
it is noteworthy that no positive means of preventing such extrusion was
demonstrated. Further, the chemical composition of the seal ants and their
stability under long-term exposure to temperature and radiation varies. It
is in the best interest of the users to identify the presence of any
potentially reactive or hazardous components of the seal ants prior to their
use on-line, and additionally to require that an evaluation be made of the
effect of the high pressure seal ant injection process on the primary
pressure boundary structure of the component being sealed.
S-2
Section 1
INTRODUCTION
To determine the state of the art in the practice of sealing on-line leaks
with regard to line conditions at nuclear power plants, a test program
sponsored by EPRI was conducted at the test faci1ities of Combustion
Engineering, Inc., Windsor, Connecticut, during the period of August, 1980,
to January, 1982. Three firms actively and competitively engaged in on-line
industrial leak sealing participated in the major program - Vendor A, Vendor
B and Vendor C. In addition, a fourth vendor (Vendor D) was invited to
participate in an adjunct test of mechanical sealing fixtures. Vendor C
declined to participate in that particular test. This report documents the
objectives and performance of the test program, and draws conclusions
regarding leak sealing techniques and materials demonstrated by the
participants.
1-1
Section 2
OBJECTIVES
The objective of the leak sealing test program was to have several
commercial vendors of the leak repair services demonstrate their products
and techniques by sealing a variety of test specimens (valves, flanges and
pipes) under different line conditions. These repairs would be evaluated in
the short and long term (up to four months) for cold leaks, seal ant
extrusion into the process stream, and ease of seal ant removal. Chemical
analyses would be used to determine the presence of potentially harmful
elements (e.g., halogens) as well as to define the stability of sealant
samples under thermal and irradiation aging. In addition, a number of
industrial users of leak sealing services was to be surveyed to gain
perspective on the performance of these repairs in the field.
2-1
Section 3
TEST PROCEDURE
Valve Leaks
3/4 in (19mm) bonnet valve with 187 IX packing; packing leak @ 600°F, 2200
psi (316°C, 15.2mPa)
2 in (51mm) bonnet valve with 1871/grafoi1 packing; bonnet leak and packing
leak at 200oF, 2200 psi (93°C, 15.2mPa)
3-1
Once the specimens were sealed they remained on-line at the designated
temperature and pressure conditions for a minimum of 48 hours. The
specimens were then cooled and depressurized to atmospheric pressure, and
checked for sealant extrusion and leakage. Certain specimens were held
aside for material tests (refer to Appendix B), and the remainder were
reinstalled on-line for longer-term durability testing.
TEST FACILTIES
Tests were conducted on two hot loops of the Nuclear Laboratories at the C-E
Engineering Development and Services Department. Leak specimens sealed at
200°F and 600°F (93°C and 316°C)5 simulating primary flow conditions
3-2
Section 4
The objective of the sealant extrusion test, which was to quantify and
relate sealant behavior to injection pressure and system temperature, was
not achieved. It was hypothesized that a family of temperature-dependent
curves relating injection pressure to cure time could be developed, which
would thereby determine a maximum safe injection rate for a given
temperature. This test was based on the belief that during the injection
process, the sealant develops a "cured front" which progresses to the
incident point of the leak. As the cured front obscures the leak, an
increase in injection pressure is noted as cured seal ant is forced into the
incidence to seal the leak.
Data obtained from the extrusion test failed to yield any meaningful
correlat ions among the parameters of interest, i.e., injection rate,
injection pressure, volume of seal ant injected, and temperature. However,
the following observations are presented which reflect the behavior of the
seal ants under the specific test conditions imposed.
VENDOR A
The seal ant extrusion test was performed by Vendor A on two separate
occasions. During the first test, attempts at injection of seal ant at
temperatures above 400°F (204°C) were made impossible by off-gassing of
4-1
cured front in the tube itself, rather than at the orifice (See Figure
4-1). At temperatures of 300°F (150°C) or below, off-gassing was less
of a problem, but curing time increased dramatically such that a single test
exceeded 8 hours. Further, it was discovered that seal ant extrusion
continued until the injection valve was shut. No reasonable curing time
would prevent further extrusion if reinjection was attempted.
Discussion among C-E, EPRI and Vendor A following the first test led to a
retest. The original test fixture (Figure 4-1) was modified to provide back
pressure, and a small vent hole was located about 1 in (25 cm) from the
orifice (see Figure 4-2). Vendor A personnel performing the test were
allowed to pump by feel, altering injecting rates as their experience
dictated. Both problems of off-gassing and continuous seal ant extrusion
failed to materialize during the retest.
When questioned about the off-gassing of the sealant during the first test
and the complete absence of this condition during the retest. Vendor A
proposed that a difference in storage conditions may have been responsible
for the change in sealant behavior. The batch of sealant used in the retest
had been kept in deep-freeze storage prior to use, in accordance with Vendor
A's standard storage procedure. The sealant initially tested, however, had
been out of freezer storage for almost a month before its use. If improper
storage can result in poor sealant performance, then users should determine
specific storage requirements and assure vendor compliance.
VENDOR B
The requirements of the sealant extrusion test were incompatible with the
on-line sealing procedures employed by Vendor B. The extrusion test was
designed to relate a maximum allowable injection over-pressure to a given
injection rate. However, Vendor B by procedure does not exceed system
pressure during the injection process, thereby reducing the possibi1ity for
4-2
sealant extrusion. Despite this procedural incongruity, the Vendor B
sealant adapted well to the test conditions, with good results at 400°F
and 600°F (204°C and 316°C). The basic sealant cures very slowly at
temperatures below 700°F (371°C), so for this test Vendor B was allowed
VENDOR C
The Vendor C seal ant compound proved to be incompatible with the conditions
of the extrusion test. At temperatures of 500°F (260°C) and above, the
4-3
In its uncured form, the Vendor C sealant is a dense, rubber-1 ike material.
After short-term exposure (48 hours) to primary coolant conditions, bulk
sealant samples lost their surface resilience, and presumably any
thermo-plastic nature.
4-4
-.37^ <f> X .0<£>7
-1^
I
CT>
VENDOR A
The first injection into the void is made through a valved port
approximately 180° from the leak, while venting through a diametrically
opposed valve. When seal ant begins to extrude through the vent, that valve
is closed, and another valve is opened. The point of injection may or may
not be changed depending on the size of the cl amp and number of injection
ports provided. Ideally, as the void is nearly filled with seal ant, the
leak path will be reduced to two adjacent valves. At this point, if the
leak is sealed by injecting through one of these valves with the other
vented to atmosphere, the possibi1ity of introducing a stringer is minimal.
Occasionally, the leak wi11 become isolated to a single port; usually an
adjacent valve is opened and the cured seal ant drilled to reestablish a vent
prior to injection. If the vent path cannot be reestablished, the vendor
injects through the final valve, which increases the possibility of
introducing a stringer. A typical injection sequence of the void (refer to
Figure 5-1) is as follows:
5-1
Injection Number Injection Port Vent
1 5 1
2 5 3
3 6 1
4 6 2
5 1 2
6 4 3
7 3 2
8 3 I
9 2 3
The initial leak in this case was between valves 2 and 3. Other valves are
utilized for providing the perimeter seal. Item 7 is the down stream
strainer used to determine if seal ant was carried into the process stream.
Reinjections of al1 or some of the ports after 1 hour is common.
Valve packing leaks are repaired by drilling and tapping into the stuffing
box, then injecting pumpable packing material until the leak is sealed and
ful1 travel is restored to the gland.
Rate and total volume are not monitored during the injection process. The
procedures demonstrated during the tests, however, call for a final
injection gun hydraulic pressure of 9000 psi (62 mPa). It is impossible to
relate this to injection or cavity pressure since the slightest restriction
in the flow path increases the hydraulic pressure dramatically. For
example, it takes 2000 to 3000 psi (13.8-20.7 mPa) pressure to push uncured
seal ant out of the gun by itself. Hydraulic pressures during initial
injection range from 4000 to 6000 psi (27.6 to 41.4 mPa). It should be
noted that these pressures refer to hydraulic injection tool pressures, and
not seal ant pressures.
5-2
VENDOR B
Because of the fluid nature of their sealant, Vendor B was able to use fewer
injection ports on their flange enclosures. The 4-inch flange required only
two injection ports, in contrast to Vendor A's six and Vendor C's eight .
Despite the installation of four injection ports on the 3/4 in (19mm) flange
enclosures (see Figure 5-2), the bulk of the sealant was injected through
the first port. After the first injection the selection of ports for
additional injections was random, but the final injection was always made
through the port nearest to the slowly diminishing leak, which typically was
situated at a stud.
5-3
If the pressure closures are designed such that the gasket is physically
retained at the pressure boundary, such as in the case of a captured gasket
or metal 0-ring, Vendor B may elect to inject directly into the damaged
gasket cavity by first drilling, tapping and installing an injection port
and valve in the area of leak. This was the method used for both 6 in and 2
in (150mm and 51mm) valve bonnet leaks. See Figure 5-3.
The clamps used for the 3/4 in (19mm) pipe specimens were unique in that
they did not require the injection of the sealant into the area surrounding
the leak. The seal ant is used as a gasket material between mating surfaces
of the two halves, while the longitudinal axis is sealed on either end by
means of a two-piece compression fitting which bolts around the pipe and
into the clamp.
VENDOR C
Vendor C flange repair fixtures (Figures 5-2 and 5-4) closely resembled
those used by Vendor B in that they fit between the flange faces, leaving
only the cavity surrounding the leak for seal ant injection. The injection
ports, however, are installed in the flange itself, rather than in the
repair enclosure. Not only does this increase the duration of the repair,
sinee injection ports can be predrilied on a flange repair enclosure, but
also the likelihood of damaging a stud.
5-4
Injection Number Injection Port Vents
1 4 1,2,6,7
2 5 1,2,3,6
3 3 1,6,7,8
4 6 1,2,7,8
Port 6 drilied out
5 6 1,2,7,8
6 7 1,2,8
Port 7 drilled out
7 7 1,2
8 6 1,2
Port 3 drilied out
9 3 1,2
Port 8 drilled out
10 8 1,2
11 2 1
Flange face peened to reduce leakage
12 1 No vent
Port 1 drilied out
The original leak in this case was between ports 8 and 1. Note that ports
are drilied out only for injection purposes, never to reestablish a vent.
The final injections were made with no vent to atmosphere except through the
path of leakage. Single cavity enclosures were also used on all 3/4 in
(19mm) pipe specimens (see Figure 5-7). These enclosures contained two
injection ports, one located directly over the leak, and the other 180°
apart. Final injections were made with no vent, and in one instance a final
injection was made with the leak already sealed. Observation of Vendor C
repairs led one to believe that their procedures do not call for any
diffusion of the leak prior to the installation of the repair enclosure. On
the first attempt by Vendor C to seal a pipe specimen, stainless steel wire
was wrapped around the pipe in the area of the leak; this had no effect on
the magnitude of the leak. Main stream extrusion was significant, and upon
5-5
disassembly it was evident that the wire had been completely displaced
during the installation of the repair enclosure. After Vendor C personnel
were made aware of this extrusion, a hose clamp was used for the final pipe
test to diffuse the leak, requiring a portion of the repair enclosure cavity
to be ground away to accommodate it. Prior to this, two other pipe leaks
were sealed with no attempts made at diffusing the leaks.
5-6
Figure 5-1. Vendor A Enclosure on 4 in Flange
5-7
Figure 5-2. Comparison of 3/4 in Mange Repair Fixtures
Figure 5-3. Vendor B 2 in Valve Repair - Note: Packing Repair
Successful; Existing Leak is in Bonnet Flange
5-9
5-10
5-11
EFFECTIVENESS OF REPAIRS
Tables 2, 3 and 4 show test results from the long-term thermal cycling tests
performed on specimens sealed by Vendor A, Vendor B and Vendor C,
respectively. It is obvious that for the sealing conditions tested no
vendor can claim consistent success. Assuming an acceptance criterion for a
successful repair of zero leakage initially, then both Vendor A and Vendor B
can claim a success rate of about 50%, with 6 and 5 of 12 specimens
perfectly sealed, respectively; Vendor C's repairs showed zero leakage in
only two specimens. If an arbitrarily selected small leakage of one gallon
per day (approximately 160 cc/hr) is acceptable, then all vendors exhibited
an improved success rate : 7 out of 12 for Vendor A , 6 for Vendor B, and 5
for Vendor C.
The longest term over which the repairs were tested on line was 14 weeks;
the specimens tested were two 3/4 in (19mm) pipes and a 3/4 in (19mm)
flange. With the exception of the Vendor C specimen which suffered the bulk
extrusion, all the pipe repairs were successful both initially and over the
14 weeks. Al1 the 3/4 in (19mm) flange repairs held for the initial 48
6-1
hours, but the Vendor A specimen ultimately developed significant leakage
(>10,000 cc/hr) by the end of the test period. In addition, the 4 in
(100mm) flanges were to have remained on 1ine for 14 weeks; none lasted more
than 8 weeks before serious leakage occurred.
Vendor A
6-2
Permanent repair of flanges and valves sealed by Vendor A could be
prohibitive, due to both sealing techniques and the sealant itself. The
liberal peering of flanges prior to sealing caused damage which would
require remachining of all flange faces sealed by Vendor A , if reuse was
contemplated. Typical damage is illustrated in Figures 6-2 and 6-3.
Disassembly of flanges and valves was extremely diffcult, due to the
concrete-like nature of the cured sealant. Although it does not adhere well
to metallic surfaces, its cohesive and incompressible nature made necessary
the cutting of valve studs and the use of a hydraulic press to remove studs
from flanges.
Vendor B
Permanent repair of parts sealed by Vendor B should not pose any exceptional
problems. Flanges were peened at their interface with the repair clamp, and
not at the mating surfaces, thereby eliminating a source of flange damage.
The cured seal ant is nonadhesive and remained relatively soft, and did not
hinder the disassembly of any test specimens.
6-3
Vendor C
The initial effectiveness of the Vendor C repairs was marginal. The 3/4 in
(19mm) pipe specimens proved to be especially difficult to repair; Figure
6-5 shows a typical leak after the Vendor C repair failed. Of repairs that
held up for the initial 48 hours, however, most continued for the duration
for the long-term tests with little or no increase in leakage.
Vendor C's demonstration of leak repairs also resulted in the most severe
case of extrusion witnessed during the test program. This occurred during
the repair of a 3/4 in (19mm) pipe specimen at 600 F (316 C). The
initial repair failed after approximately one hour on-line. The repair
fixture was removed, cleaned, reinstalled and finally reinjected. After 48
hours on-line, when the test specimen was removed for hydrostatic testing,
two separate slugs of seal ant were discovered in the pipe downstream of the
repair. One slug was caught in a 90° pipe bend about 4 in (10 cm) away
from the test specimen, and the other slug was lodged in the test pipe
itself. Both slugs are shown in Figure 6-5. The test specimen was
sectioned for examination, and is shown in Figure 6-7. Note in the
photograph the displaced wire wraps in the vicinity of the leak, as referred
to in Section 5. From examination of the slugs and approximating their
3
volume as 0.5in (8 cc), it appears that the extrusions were produced
separately, one for each attempted repair.
LINE CONDITIONS
TEST SPECIMEN I.D.# DURING SEALING VENDOR A VENDOR B VENDOR C
3/4" Pipe Specimens:
with 1/64" dia. hole 1 540°F, 2200 psi 0.0 (0.0) 0.0 (0.0) 4,360 (1.15)
200°F, 2200 psi ^51,000 (13.47)
with 1/32" dia. hole 2 0.0 (0.0) 0.0 (0.0)
with 1/16" dia. hole 3 600°F, 2200 psi 0.0 (o.o) 0.0 (0.0) (2)
with 1/16" dia. hole 4 200°F, 2200 psi 0.0 (0.0) 0.0 (0.0) 10 (<0.01)
6" Valve 5 600°F, 2200 psi 2,720b (0.72) 8,000a (2.11) 10afb (<0.01)
cr> 3/4" Valve 6 600°F, 2200 psi 0.0 (0.0) 240a (0.06) (3)
^ 2" Valve 7 200°F, 2200 psi 0.0 (0.0) 740b (0.19) 40b (0.01)
3/4" Flange 8 200°F, 2200 psi 80 (0.02) 0.0 (0.0) 0.0 (0.0)
3/4" Flange 9 600°F, 2200 psi 200 (0.05) 1,120 (0.29) 6,000 (1.58)
3/4" Flange 10 600°F, 2200 psi 3,440 (0.91) 120 (0.03) 13,000 (3.43)
3/4" Flange 11 600°F, 2200 psi 13,240 (3.49) 1,600 (0.42) 19,000 (5.02)
4" Flange 12 600°F, 2200 psi 72,314 (10.10) 9,000 (2.37) 5,000 (1.32)
6" Valve Leakage after 2 wks on-1ine 9,720b (2.56) 13,200a(3.48) 100a,b (0.02)
(1) Removed from line conditions after 24 hrs; 1500 psi was maximum hydrostatic pressure attainable
(2) Could not be hydrostatic tested without disturbing bulk extrusion (see text)
(3) Negligible: leakage from packing, about 1 drop/min.
(a) Packing leak
co 00 CO ^
2: O CO 2: Q CO 2: 0 CO
0 UJ >- O UJ >- O UJ >-
LEAKAGE HH s: LU LEAKAGE t“-i UJ LEAKAGE (—1 UJ LEAKAGE
{
— C£ ^ ^
cc: 1—QC ^
LINE CONDITIONS AFTER C O AFTER <c 0 AFTER < O AFTER
01 U- LU u.
cc: uj QC U- UJ
DURING 48 HR LONG-TERM LU LU 2 WEEKS UJ OC UJ 8 WEEKS UJ DC UJ 14 WEEKS
Q- UJ CO A- uj co CL UJ CO
SPECIMEN # SEALING cc/hr LINE CONDITIONS 0 a. ^ cc/hr So- — cc/hr O CL'— cc/hr
OPERATIONS
OPERATIONS
OPERATIONS
(SEE KEYS)
(SEE KEYS)
(SEE KEYS)
PERFORMED
PERFORMED
PERFORMED
LEAKAGE LEAKAGE LEAKAGE LEAKAGE
LINE CONDITIONS AFTER AFTER AFTER AFTER
DURING 48 HR LONG-TERM 2 WEEKS 8 WEEKS 14 WEEKS
SPECIMEN # SEALING cc/hr LINE CONDITIONS cc/hr cc/hr cc/hr
OPERATIONS
OPERATIONS
(SEE KEYS)
OPERATIONS
(SEE KEYS)
(SEE KEYS)
PERFORMED
PERFORMED
PERFORMED
LEAKAGE LEAKAGE LEAKAGE LEAKAGE
LINE CONDITIONS AFTER AFTER AFTER AFTER
DURING 48 HR LONG-TERM 2 WEEKS 8 WEEKS 14 WEEKS
SPECIMEN # SEALING cc/hr LINE CONDITIONS cc/hr cc/hr cc/hr
6-9
Figure 6-2. Peem'ng Damage on 4 in Flange Sealed
By Vendor A
Briaa—
Figure 6-3. Close-Up Of Peening Damage On 4 in Flange Sealed Vendor A
6-10
Figure 6-4. Sealant Extrusion Found In Pipe And Strainer Downstream Of 3/4 in
Flange Sealed By Vendor B
6-11
Figure 6-5. Leak In Vendor C Line Enclosure Prior To Termination Of Test
6-12
Figure 6-6. Vendor C Line Enclosure With Extruded Sealant Slugs
6-13
6-14
Figure 6-7. Section Through 3/4 in Pipe Sealed By Vendor C, Showing Bulk Extrusion
Section 7
During the course of the leak sealing program, both Vendor A and Vendor B
suggested that the type of repair fixture used to repair pipe leaks could be
successfully applied to leaking valves and flanges. The general design
features of such a fixture include a void chamber to accommodate the flange
(or valve), and a perimeter seal on the repair fixture itself. This repair
The three vendors participating in the leak sealing tests, plus a fourth
vendor, were invited to demonstrate their techniques for "mechanical11 or
"semi-mechanical" repair of on-line leaks. Test requirements were that one
3/4 in (19mm), 1500-pound flange would be sealed at line conditions of
620°F and 2200 psi (327°C, 15.2 mPa), and that the injection of sealant
between the two flange faces would not be necessary. Given these
conditions. Vendor B and Vendor A agreed to participate, while Vendor C
declined, citing limitations of this type of repair under the ASME Boiler
and Pressure Vessel Code. A fourth vendor. Vendor D, also agreed to
participate. The individual repairs are discussed separately below.
VENDOR A
The repair fixture used by Vendor A is shown installed in Figure 7-1. Prior
to assembling the fixture around the flange, Vendor A followed their
previously demonstrated procedure of first diffusing the leak by peem'ng the
flange. This was followed by wrapping the bolt circle with stainless steel
7-1
wire until it approximately equal led the f1ange O.D. The fixture was then
assembled about the flange, and pumped with sealant. The duration of this
initial repair was about 6 hours. After 14 hours, the fixture was repumped
with sealant for 2 hours.
After 48 hours at line conditions, the fixture was taken off-line, cooled
and tested for leaks. Zero leakage was measured at 2200 psi (15.2 mPa).
VENDOR B
The Vendor B fixture, as shown assembled in Figure 7-3, was the smallest and
the lightest (50 lb (22.7 kg)) fixture demonstrated, and was the only one
with a single perimeter seal. Duration of initial repair was 3 hours, and
repumping for 1 hour was performed 10 hours after the initial repair. After
approximately 36 hours on-1ine, a significant leak occurred near a stud, and
continued until the fixture was taken off-1ine. (Under normal circum
stances, al1 vendors are available for a repump within 48 hours of the
initial repair. Hoi iday schedules of both Vendor B and C-E eliminated the
opportunity for a 1 ate repump.) Leak testing at ambient temperature showed
the leak rate to be 12,800 cc/hour at 2200 psi (15.2 mPa).
When the Vendor B fixture was disassembled, the reason for the substantial
leak was discovered. Again, due to hoiiday schedules and the desire to
complete testing prior to the end of the calendar year, the Vendor B
enclosure was designed from a drawing of the flange and pipe, rather than
7-2
from actual field measurements. The pipe actually tested had an O.D. 5 to
10 mils (0.13-0.25 mm) 1arger than that specified in the drawing sent to
Vendor B. This mismatch of pipe and fixture prevented f1 at contact between
the upper and lower flange faces of the repair fixture, especially near the
pipe/fixture intersection, thereby shortening the path from void to studs.
A photograph of the disassembled fixture is shown in Figure 7-4, and the
flange is shown removed from the fixture in Figure 7-5.
VENDOR D
The Vendor D mechanical sealing fixture was the only one tested which
incorporated separate, inner and outer (removable asbestos) seals in
addition to an intermediate groove for seal ant containment. This design
feature serves as a reasonably effective means of containing seal ant away
from the leaking flange, helping to insure that no seal ant is extruded into
the process stream. The photographs of the disassembled fixture in Figure
7-7 clearly show the absence of seal ant in the void chamber.
The f1ange repair with the Vendor D fixture failed for the same reason as
did the Vendor B unit, which was an over-sized pipe with respect to the pipe
clearance manufactured in the fixture. As with the Vendor B fixture, true
pipe dimensions 1arger than those stated on the drawing provided to Vendor D
were responsible. The net result was a cold leak rate in excess of 15,000
7-3
cc/hour at 1800 psi (10.2 mPa). Vendor D was willing to provide a new
fixture of the correct size for this application, accommodating the true
pipe diameter, but additional test time was not available.
7-4
Figure 7-1. Vendor A Mechanical Sealing Fixture, Installed
7-5
Figure 7-2. Vendor A Mechanical Sealing Fixture, Disassembled After Test
7-6
Figure 7-3. Vendor B Mechanical Sealing Fixture
7-7
Figure 7-4. Vendor B Mechanical Sealing Fixture, Disassembled After Test
7-9
Figure 7-6. Vendor D Mechanical Repair Fixture, Installed
7-11
Section 8
It was not the objective of the program to determine which, if any, of the
vendors provided the most effective and consistent leak repairs. Rather,
the demonstrations by the participating vendors and subsequent long-term
tests offered substantial insight into the state of the art regarding such
repairs. As such, the program allows the following conclusions and specific
recommendations to be made.
CONCLUSIONS
8-1
2. Sealant extrusion into the process stream was infrequent, but
observations made during the test program suggest that such extrusions
can not be positively prevented. Mechanical sealing fixtures (as
described in Section 7) may significantly reduce the risk of such
extrusion.
7. Valve repairs were generally less successful than repairs of pipes and
pipe flanges. This may be attributable to the fact that most of the
valves were repaired without the use of enclosures, but rather by
injecting sealant or pumpable packing material into the stuffing boxes
directly. The effectiveness of these repairs is thus more closely
related to the performance of the sealant (or pumpable packing material)
itself.
8-2
RECOMMENDATIONS
4. The design basis for the fixtures employed should be considered by the
user as these sometimes rather massive structures do become a new
pressure boundary once the repair is effected. Further, if the repair
fixture captures injected sealant between flange faces, the additional
loading on the flange studs due to injection pressure (above system
pressure), possible increase in effective sealing diameter, and
mechanical sealing operations must be considered.
8-3
Section 9
REFERENCES
9-11. Video Tape Recordings of Vendor A Leak Repairs, Tapes A-l, A-2, and
A-3.
9-1
APPENDIX A
VENDOR SURVEY
Respondents were questioned about the following: which leak repair vendor
was selected; the frequency of use; the types of components sealed; line
conditions at the leak; and the general performance of the repair -
effectiveness, presence of stringers and/or effect on system chemistry,
difficulties with permanent repair, etc.
The components which most frequently required leak sealing were valves, from
1/2 in to 30 in (1.2 to 76 cm). Flanges were the next most common source of
leakage, with only a few users reporting pipe leaks. Line conditions for
the repairs ranged in temperature from 250°F to 1250°F (120°C to
675°C) and in pressure from 150 to 2600 psi (1 to 18 mPa). Both thermal
Respondents on the whole felt that vendor repairs were generally effective,
and they recognized the temporary nature (6-12 months) of the repairs.
Typically, 20% of all repairs required reinjection well after the initial
A-l
repair was made. High temperatures, high pressures, and especially thermal
cycling were cited as the most common causes of repair failure which
necessitated reinjection. However, some users reported valve repairs which
had lasted 2-1/2 years before failure.
No users reported any serious doubts about the chemical composition of the
sealants used, generally trusting the vendor's judgement as to the
suitability of the sealant used for the specific application. No chemical
analyses of sealant materials (to determine system compatibility) was
demanded of the leak repair vendors, or performed by the customers. Effects
of repairs on process (plant) chemistry were either unnoticed pr
nonexistent. However, about 20% of the respondents reported evidence of
stringers in their systems as a result of leak repairs.
In contrast to observations made during the leak sealing test program, the
removal of cured sealant from parts sealed by all three vendors in field
applications presented no special problems. In contrast, flanges and valves
sealed by Vendor A during the test program had proven to be almost
impossible to disassemble without damage.
It should be noted that only firms which had employed leak repair vendors
were included in the survey; some firms undoubtedly decline to inject
sealants to repair their leaks. With this in mind, it is perhaps not
surprising that all respondents felt the concept of on-line leak sealing was
cost effective, and that results were at least satisfactory. Vendor C
enjoys the largest share of the leak repair market among the users surveyed,
with Vendor A and Vendor B sharing the balance. Only two respondents had
used more than one vendor, so no conclusions can be drawn about customer
preference.
A-2
APPENDIX B
Section B-1
INTRODUCTION
PROCEDURES
The sequence of sealant tests was performed per the basic diagram in Figure
B-1. Individual test procedures are detailed in the following sections.
dishes, and were weighed before and after curing to determine weight
loss.
B-1
Irradiation of Sealant
noted in the discussion of the individual sealants. The dose rate for
these samples was 0.667 Mrad/hr for 15 hours.
The primary coolant in which each of the sealant samples was irradiated,
retained and subsequently analyzed for Teachable elements.
Thermal Aging
Elemental Analysis
The sealants and primary coolant samples were analyzed for elemental
composition at National Spectrographic Laboratories in Cleveland, Ohio.
Individual analysis techniqes are described as follows:
B-2
Total halogens in sealant: Samples were pyrolytically decomposed using
externally-heated furnace with an 0^ gas sweep into a liquid
caustic trap. Halogens were measured with specific ion electrodes per
ASTM Dll79-80 (B).
Mercury: Samples were analyzed for mercury by the Cold Vapor Generation
Method according to EPA 245.1.
Total lead, copper, zinc tin and cadmium: These metals were analyzed by
wet ashing around a gallium oxide carrier, followed by emission
spectroscopy.
Coolant Analysis
An analysis was run on the coolant used for the sealant environment
during irradiation. Analytical measurements were made on all coolant
samples, including the blank, after irradiation. Except as noted in
B-3
Table B-3, no increases in the elemental impurity levels of the coolant
samples, as compared with the original solution, were measured. This
indicates that no measurable quantities of impurities (except as noted)
were extracted into the coolant during irradiation.
Vendor A
This material was stable with respect to heat both during the initial cure
(20 hours at 475°F) and the 8 week, 400°F thermal aging following
Vendor B
The Vendor B sealant exhibited very poor stability during the thermal
(curing and aging) cycles. While curing, this material lost over 30% of its
initial weight, a brown viscous oil distilled out of the sample, and a great
deal of shrinkage was noted. During the post-irradiation thermal aging, an
additional weight loss of 22% was measured, resulting in a total weight loss
of over 50%.
B-4
Regarding impurities, the Vendor B sealant has very high levels of chlorine
and sulfur, and high levels of fluorine. Significant amounts of both
chlorine and fluorine also leached into the cool ant during irradiation at
primary conditions.
Vendor C
During the initial cure, the Vendor C sealant gained weight, indicating that
an oxidative curing reaction may have occurred. The weight change during
the 8-week thermal aging showed a moderate loss.
Elemental impurity levels were general ly low, although the chlorine levels
are above Combustion Engineering criteria (refer to Table B-4). No other
impurities were present above the 1imits of detectability.
B-5
Table B-1
Total F * 76.1
(2) k k
10 (2)
Total Br 10 * k
(2) k
(2) k
Total I 10 * k
(2) k
(2) k
Leachable F 10 * k k k k k
Leachable Cl 10 * 167 k
165 k k
Leachable S 100 * * k * k k
P 10 •k k k * k k
k k k k k k
Eg 0.5
k k k k k k
Pb 10
k k k k k
Cu 10 k
k k k k k
Zn 10 k
k k k k k
Sn 10 k
k k k k k k
Cd 50
B-6
Table B-2
10 175 2354
Total F (2) 250 (2) (2)
4 1130'
Total Cl 10 1960 1550 (2) 720 205
Total Br 10 (2) *
(2) * (2) *
Total I 10 (2) *
(2) k
(2) *
0.5 ■k * k * * *
Hg
Pb 10 k * k * k k
k k
Cu 10 21 ■k
20 30
Zn 10 * k k * k k
Sn 10 * k k k k k
* k k k k k
Cd 50
B-7
Table B-3
Total F 10 (2) ■k * k
(2) *
Leachable F 10 * * * * k k
Leachable S 100 * * * * k *
P 10 * * * * k *
Hg 0.5 ■k * * k k k
Pb 10 * * * k k k
Cu 10 94 40 92 20 84 38
Zn 10 ■k * * k * k
Sn 10 19 * 15 k
14 k
Cd 50 * * ■k k * k
B-8
Table B-4
Spent Fuel or
Impurity Reactor Intervals Steam Generator Refueling Pool
Total F 50 1000 50
Total Br 50 100 50
Total I 50 100 50
Leachable F 50-100* 10 10
Leachable Cl 50-100* 10 10
Leachable Sulfur 50 50 50
*Depending on application
B-9
CURE SEALANT
SPECIMENS„
INTRODUCTION
PROCEDURES
All flanges were sealed on-line with internal pressure and temperature of
the borated water test medium at 620°F, 2200 psi (327°C, 15.2 mPa).
After 48 hours on-line, the test specimens were cooled, depressurized, and
hydrostatically tested for leaks at room temperature. Flanges were aged in
groups of three at 300°F, 45Q°F, and 750°F (149°C, 232°C, and
398°C) for 8 weeks total. After the first two weeks, and at subsequent
two-week intervals, the flanges were again checked for leaks, and hardness
measurements were taken on samples of the sealant.
Leakage measurements for the aged flanges are shown in Table B-5, and
hardness readings for the aged sealant specimens are given in Table B-6.
B-11
Sealant hardness measurements varied during the aging period. Only Vendor A
sealants uniformly increased in hardness at al1 temperatures. Seal ants from
Vendor B and C reacted similarly, increasing in hardness with aging at
300°F, but both curiously decreasing in hardness with aging at 450°F.
A uniform trend relating sealant hardness (or change in hardness) with the
rate of f1ange leakage was not clearly defined. It had been hypothesized
that as the sealant materials hardened with thermal aging, any elastomeric
properties would diminish, and leakage would increase. As stated above,
flange leak rates showed a general increase during the aging period, but
this trend does not appear to be associated with the change in seal ant
hardnesses.
B-12
ft
Table B-5
Initial Leakage
Vendor Aging After 48 hrs.
& Specimen No. Temperature On Line 2 weeks 4 weeks 6 weeks 8 weeks
9 750°F 200 40 0 0 0
B-1 3
Vendor Agi ng
& Specimen No. Temperature 2 weeks 4 weeks 6 weeks 8 weeks Scale
11 750°F (1) - - -
NOTE:
(1) Sealant sample broke down into non-cohesive powder.