ELECTRICAL MOTOR TEST REPORT
Customer : Philippines Mining Service Corporation
Address : Pugalo, Alcoy, Cebu 6023
Work Description : EMERGENCY SERVICING / RECONDITIONING OF 1 UNIT 30 KW,
INDUCTION MOTOR, 440v, 3PHASE AND SUPPLY OF BRAND-NEW BEARING. PPR NO. 32278
UNIT DATA:
Horsepower 40 HP / 30 KW Hz 60Hz
Type CYCLO DRIVE RPM 1760
Make TECMESH MACHINARY INC. Drive End 312ZZ
Voltage 220/380/440 VAC Non Drive End 6310ZZ
Phase 3 SN C12007-181860
ELECTRICAL TEST REPORT:
BEFORE SERVICING / RECONDITIONING
I. MEGGER/POLARIZATION INDEX (BEFORE RECONDITIONING) Date: January 13, 2022
A. Instrument Used: 250V/500/1000V
Specimen Impressed Voltage 1 minute 10 Minutes Remarks
Stator 1000 MΩ 0.00 MΩ 0.00 MΩ DANGEROUS
Rotor - - - -
10 minutes reading
Guide 1. 1 minutes reading
2. Table of Evaluation:
Dangerous ……………………Less than 1.0
Poor ………………………….1.0 – 1.1
Questionable …………………1.1 – 1.25
Fair ..........................................1.25 – 2.0
Good ........................................More than 2.0
AFTER SERVICING / RECONDITIONING
II. MEGGER/POLARIZATION INDEX (AFTER RECONDITIONING) Date: January 16, 2022
A. Instrument Used: 250V/500/1000V
Specimen Impressed Voltage 1 minute 10 Minutes Remarks
Stator 1000 V 600 MΩ 2000 MΩ 3.3 (VERY GOOD)
Rotor - - - -
III. WINDING RESISTANCE TEST
BEFORE SERVICING / RECONDITIONING
Instrument Used: FLUKE
STATOR ROTOR
L1-L2 0.2 Ω - -
L2-L3 0.2 Ω - -
L3-L1 0.2 Ω - -
AFTER RECONDITIONING
Instrument Used: FLUKE
STATOR ROTOR
L1-L2 0.2 Ω L1-L2 -
L2-L3 0.2 Ω L2-L3 -
L3-L1 0.2 Ω L3-L1 -
IV. MECHANICAL INSPECTION:
Specimen Clearance Remarks
Bearing housing drive side end Tight fit Thorough cleaning done
Bearing housing, non-drive Tight fit Thorough cleaning done
Bearing journal drive side end Tight fit Thorough cleaning done
Bearing journal non-drive end Tight fit Thorough cleaning done
V. WORKS TO BE DONE:
AFTER DISMANTLE
1. As observed water and muds were seen inside the motor. Thorough cleaning was done in
an area inside and outside the unit.
2. Motor cleaner / de greaser was sprayed to remove all contaminant.
3. Continuous heating for 72 hours was done until megger reading reach infinity.
4. Varnishing of rotor and stator coil.
5. Red varnish was applied seal of the coils.
6. Cleaning of all motor accessories.
7. Cleaning of motor external parts and re painting.
8. Install of brand-new bearing.
9. Assemble back the unit.
10. Motor testing done
VI. RECOMMENDATION:
This unit was put back in a good condition and is ready for no load testing and
can be use on normal plant operation.
Submitted by:
CLARITO B. DACUA
General Manager
BEFORE
AFTER