Turbo Expander Compressor
Turbo Expander Compressor
by
Frank Davis
Engineering Consultant
Doha, Qatar
Reza Agahi
Consultant
Irvine, California
and
Randy Wu
Senior Engineer
GE Oil & Gas
Rancho Dominguez, California
Frank Davis is an Engineering Consultant with ExxonMobil, Randy Chih-Chien Wu is a Senior Engineer with GE Oil & Gas
assigned to Ras Laffan LNG Company Ltd., in Doha, Qatar. He has Operations LLC-North America, in Rancho Dominguez, California.
more than 30 years of experience in the field of rotating machinery. He began his career with Rotoflow Corporation (now part of GE Oil
Mr. Davis specializes in project engineering for machinery & Gas) as Thermodynamic Design and Test Engineer for expander
applications, bid reviews, and machinery acceptance testing. After and compressor products. In his 19 years of working experience, he
20 years machinery engineering experience with Exxon and Mobil has been involved in various disciplines in designing and developing
Corporations, he was a member of the Project Task Force managing of expander and compressor products. His current responsibilities
the engineering and construction of four LNG plants in the State of are focusing on risk review and NPI activities as well as test and
Qatar over the past 10 years. He has developed specifications, commission operation of expander and compressor product.
completed bid reviews, and followed manufacturing, testing, and Mr. Wu received a B.S. degree (Physics and Mechanical
participated in the startup of more than 40 machinery trains including Engineering, 1976) from Chung Yuan University and an M.S. degree
65 MW gas turbine driven refrigeration compressors and gas (Mechanical Engineering, 1983) from the University of Nebraska at
expander/compressor units. Lincoln. He is a member of ASME.
Mr. Davis received a B.S. degree (Mechanical Engineering, 1966)
from New Jersey Institute of Technology and is a registered
Professional Engineer in the State of New Jersey. INTRODUCTION
The application of the turboexpander in natural gas processing
Reza Agahi is a Consultant, in Irvine, and the petrochemical industry had its beginning at a small gas
California. He recently retired after 33 years plant in Southwest Texas where Dr. Judson S. Swearingen installed
with GE Rotoflow where he last served as the first natural gas turboexpander (Swearingen, 1999).
Director of Marketing, Sales, and Turboexpander technology has developed considerably in the
Commercial Operations. Dr. Agahi has last 40 years. For example:
taught in universities in Southern California • Advances in fluid dynamics theory and computational fluid
and has authored more than 40 articles and dynamics have made it possible to design a turboexpander with
papers in system engineering and turboma- high isentropic efficiency and performance predictability;
chinery applications. He is the inventor and
coinventor of several GE Rotoflow Patents. • Progress in rotordynamics evaluation and modern finite element
Dr. Agahi received B.S. and M.S. degrees (Mechanical analysis capabilities have resulted in more reliable turbomachinery.
Engineering, 1968) from Tehran University, and an M.S. degree • Increase in demand and economies of scale have resulted in
(1974) and Ph. D. degree (Operations Research and Systems natural gas processing and petrochemical plants becoming larger
Engineering, 1977) from the University of Southern California. and larger (Figure 1) (Agahi, 2003).
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82 PROCEEDINGS OF THE THIRTY-FIFTH TURBOMACHINERY SYMPOSIUM • 2006
EQUIPMENT The TEC speed was ramped up at 10 percent increments until the
speed closely approached the trip speed of 12,400 rpm and remained
The major components and supporting equipment in this test
at that speed for 15 minutes. Then the turboexpander compressor
loop are listed below:
speed was reduced to a maximum continuous speed (MCS) of 11,813
• Residue gas compressor, centrifugal compressor driven by a GT rpm for two hours. The test loop equilibrium state was achieved by
slowly adjusting the recycle valves of the recompressor and residue
• Residue gas compressor aftercooler gas compressor. The turboexpander compressor speed was further
• Residue gas compressor auxiliary support system reduced to the normal speed of 11,250 rpm and operated at this speed
for another two hours. At the end of this test run, the turboexpander
• Test loop piping compressor speed was gradually increased to the shutdown speed
• Flow measuring devices and the turboexpander compressor tripped on high speed. The
• Pressure measuring devices turboexpander compressor rotor coasted down under normal
conditions, i.e., the active magnetic bearing system was in levitating
• Temperature measuring devices mode during coastdown. Table 4 shows a sample of the FLFST
• Pressure transducers, cabling, data acquisition/analysis equipment parameters that were monitored.
• Startup seal gas supply, instrumentation air, etc. Table 4. A Sample of Test Parameters Monitored/Recorded.
• Gas analyzer and reporting system
• Vibration recording and analyzing equipment compatible with
active magnetic bearing system
• Residue gas compressor inline inlet strainer (60 mesh)
• Noise meter
The auxiliary equipment and components were as follows:
• Turboexpander compressor package with control system,
including active magnetic bearing signal interlock with test facility
and startup seal gas supply
• Expander bypass, Joule Thompson (JT) valve
• Expander inlet quick shutoff valve The turboexpander compressor was restarted and the speed was
• Compressor surge control system and recycle valve increased to 10,550 rpm for about 15 minutes in order for the
system to reach thermal equilibrium. A special method was applied
• Check valve downstream of the recompressor to bypass the active magnetic bearing controller and completely
• Expander inline inlet strainer (60 mesh) disable the AMB amplifiers in order to activate delevitation.
• Compressor inline inlet strainer (20 mesh) INLET GUIDE VANE SENSITIVITY
The majority of the operating parameters such as flow rates, AND FLOW CONTROLLABILITY
pressures, temperatures, vibration, etc., were monitored and logged The turboexpander compressor flow is linearly proportional to
by the automatic data acquisition system. the opening of its inlet guide vanes except in small opening and
Considering the practical aspects of the FLFST, some design full open positions. By controlling the sensitivity of the inlet guide
parameters could not be simulated. Figure 5 shows process vanes to within 1 percent, i.e., deviation between process signal to
parameters that were different during the FLFST compared to the inlet guide vanes and feedback signal to actuator system, it could
normal site conditions. be demonstrated that the expander flow controllability is within 1
percent of the total flow. As the trended data in Figure 6 show, the
differences between the inlet guide vane input signals and the
corresponding feedback signals were mostly less than1.0 percent
from ramp up to the FLFST condition. It is interesting to note that
the injection of additional fluid to increase the test loop pressure
did not influence the inlet guide vane sensitivity or flow
controllability. The inlet guide vane sensitivity remained within
1.0 percent even when the expander inlet pressure was increased
to 64 barg (928.2 psig).
FLFST Operation
Before startup, the test loop was pressurized to 24 barg (348.1
psig). The test header pressure reached 52 barg (754.2 psig) after the
residue gas compressor developed a stable pressure. Flow was
admitted to the turboexpander compressor by opening the inlet guide
vanes and closing the JT valve simultaneously. The recompressor
antisurge valve was at the full open position at the startup. The
antisurge valve began closing to load up the recompressor when the
turboexpander compressor speed reached approximately 5000 rpm. Figure 6. IGV Sensitivity Analysis.
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FULL LOAD, FULL SPEED TEST OF 85
TURBOEXPANDER-COMPRESSOR WITH ACTIVE MAGNETIC BEARINGS
AMB AUXILIARY BEARING LANDING TEST Table 5. Comparison of Radial and Axial Air Gap Before and After
Landing Tests.
Auxiliary bearings support the turboexpander compressor rotor
when it is not levitated. Another function of the auxiliary bearings
is to catch the rotor upon loss of the magnetic field resulting in
delevitation as the machine coasts down from full load and full
speed (FLFS) to a full stop. To demonstrate the functionality of the
auxiliary bearings and show their ability to support the rotor upon
delevitation at FLFS, landing tests were performed during tur-
boexpander compressor shop tests. To implement this test, the
turboexpander compressor speed was increased to 10,550 rpm, and
then the expander was delevitated by intervening with the active
magnetic bearing control system. The delevitation signal shut off
the expander inlet quick shutoff valve and opened the JT valve. The
active magnetic bearing controllers were bypassed by introducing
jumpers in the control cabinet. As a result, all radial and axial
The tear down and inspection showed that there were light
amplifiers were disabled, and the rotor landed on the auxiliary
touches on the compressor impeller blade tips. The rest of the
bearings and coasted down to a complete stop. For both landings,
rotor and its corresponding stator parts such as the expander
it took approximately 2.4 seconds from the rotor landing until the
wheel, shaft seals, sensor rings, thrust disk, and magnetic
quick shutoff valve shut off; it took 4.6 seconds for the turboex-
bearings were found to have no touch marks and were in
pander compressor to coast down to a complete stop; the rotor
excellent condition.
landed in the auxiliary bearings for a total of 7.0 seconds; and rotor
There were light marks on the ball bearing inner rings and
whirling stopped within 4.0 to 4.2 seconds. Figures 7 and 8 provide
landing sleeves in both radial and axial surfaces but the ball
detailed records of these tests.
bearings could roll freely.
ACTIVE MAGNETIC BEARING ROTOR VIBRATION
Before spinning the residue gas compressor for the FLFST,
fine tuning of the active magnetic bearings, clearance, and
tuning checks were carried out to ensure that the air gaps were
consistent with the design values, transfer functions were up to
date, and all the required securities were set correctly. The
bearing system was equipped with antivibration rejection and
automatic balancing system logic. The antivibration rejection
activation deactivation limits were set at 3400 and 4600 rpm,
respectively. The rotor first critical speed was estimated to be
approximately 37 Hz. At higher speeds the automatic balancing
system took over the control function. These two systems
ensured that the active magnetic bearing rotor always rotates
around its inertia center. Figure 9 shows the turboexpander
compressor rotor vibration throughout the course of the FLFST
including both landing tests. The higher rotor vibration was
Figure 7. First Landing Test. observed during ramp up, at a speed range between 6,000 to
9,000 rpm. The highest vibration reached 50 mm and was
mainly in the subsynchronous spectrum, from approximately
37 percent to 44 percent of the synchronous frequency, and
occurred only during the startup period. The vibration at this
level was considered normal compared to the alarm setting of
90 mm. The tangential velocity component, i.e., exit from
the inlet guide vanes, could cause swirling around the
turboexpander wheel and resonate at subsynchronous
frequencies. At FLFST conditions, subsynchronous displacements
were almost nonexistent and overall vibration levels were about
15 µm. The axial vibration was about 13 mm.
Before and after the landing test, both the radial and axial air
gaps between the rotor and auxiliary bearings were measured,
compared, and contrasted (Table 5). The data showed that there
were no changes in gap dimensions after two landing tests. Figure 9. Rotor Total Displacement/Vibration.
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86 PROCEEDINGS OF THE THIRTY-FIFTH TURBOMACHINERY SYMPOSIUM • 2006
The active magnetic bearing current chart, Figure 10, shows the
current for each bearing during the FLFST. The relatively flat curves
indicate that the rotor was quite stable at the FLFST conditions.