LSS Project
LSS Project
Team Members Sukumar (General Manager, CFL Chennai), Rakkumuthu (Production Head, CFL, Chenna),
SenthilKumar (Quality, CFL, Chennai),
Project Selection Matrix
2
Project Selection Matrix
3
Define Measure Analyze Improve Control 4
Project Charter
Project GB/Ennore/ Green Belt Balaji D Unit / Machining / Quality
Code 2011/A Function
Mentor / Sponsor AL CQE-R. Sethuraman / P. Dakshinamurthy Gemba Machining Unit
Project Definition
Project Title To reduce Flange Coupling dimensional variations
Problem Repeated issues (during March 2011 – Aug 2011) arising out of dimensional variations with Flange Coupling
Definition component at the customer end.
Scope Finishing Operation 1 and Operation 2 done in CNC in Machining unit
Goal Metric PPM From 2,303 PPM To 100 PPM Target 0 PPM
Statement (Entitlement)
Tangible Money 1. Reducing Rejections and there by Other 1. Customer satisfaction will be improved
Benefits Savings / ECU reducing loss from it Tangibles
2. Self morale will be improved
Customers Ashok Leyland
Targets Actual
• PPM of less than 100 • Customer PPM: 0 as of Jan 2013
• 80% reduction of in process • 100% reduction in, in-process
Results rejections due to shaft OD oversize rejections due to Shaft OD o/s or
/ undersize u/s
• 80% reduction in overall in in-
process rejections.
Charter P
Define
preparation A
P
Process Map
A
P
Measure MSA
A
Attribute P
P-chart A
Scatter, Box P
plots A
Analyze Customer P
onsite Visit A
Hypothesis P
tests A
Hypothesis P
Tests A
Improve
Process P
Capability -
New A
P
Control Plans
A
Control
P
A Define
Define Measure Analyze Improve Control 10
Project Reviews with AL
Number of Parts 10
Tolerance 0.039
No Actions taken
Number of Appraisers 3
Number of Parts 10
Tolerance 0.039
Type of Is the
Data Who will Method of
KPIV / Data Sample Measurement
Process Source Collect the Collecting
KPOV (Variable / Size System
and Location Data? data
Discrete) Capable?
Machining
OD Micrometer
Cylindrical Unit - CNC Padmana Yes
(34.936 - Variable 50 25-50 mm
Grinding Line bha
34.975)
From the graph, it appears that we cannot narrow down the cause to any shift/operator/machine
Define Measure Analyze Improve Control
In Process Rejections (OD) Analysis
Data
Offset issue seems to be primary reason for OD variation, and it appears to happen across
shifts/machines.
Define Measure Analyze Improve Control
In Process Rejections (OD) Analysis
Inability
Data to identify Insert worn out, leads to oversized
components;
Inability to set the right offset after tool change, leads to
undersized components;
Currently no mechanism to keep track of the number of
components that are processed for that operation;
Currently no instruction to the operator, as to when to change
the insert for 1st operation. Onus is on the operator to keep track
and also monitor the dimension of the components and then
change the insert accordingly.
Assembly Fitment 6 Improper loading 4 Trained operator Line 3 72 Taper Mandrel used
30.CNC FINISHING 2nd
Run out 0.1 variation Problem at customer Inspection Report to check down the P.Rakku muthu 12/15/2012 6 3 2 36
OPERATION
end Run Out Variation
using Dial Gauge
concentricity
Flange Coupling
Painting Issue
Flange Coupling
Damage Issue
Implementation Date:
15/09/2011
Define Measure Analyze Improve Control
Define Measure Analyze Improve Control 63
Control Chart – Before Vs After – In-
House
Data
Data
Data
Data
After completion of
the insert life, CNC
m/c will raise an
alarm
Work Instructions in
local language for the
operator
IR
OUTER DIAMETER 43
LENGTH 118
OUTER DIAMETER 98
OUTER DIAMETER 53
FIR
OUTER DIAMETER 43
LENGTH 118
OUTER DIAMETER 98
OUTER DIAMETER 53
RIR
OUTER DIAMETER 39.80 / 40.20 VERNIER
BEVEL PROTRACTOR &
CHAMFER 2 × 45°
CNC 1ST OPERATION WNMG 080412 FACING & VERNIER
40 5 NOS PER HOUR LIR QUARANTINE ADJUST & RECHECK
( ROUGH MACHINING - I ) TURNING TOOL
LENGTH 40.50 / 41.00 VERNIER
60 CASE HARDENING PIT TYPE FURNANCE HARDNESS 227/277 BHN BRENELL HARDNESS TESTER 5 Nos Per LoT RIR & SIR QUARANTINE ADJUST & RECHECK
85
Lessons Learnt