Mandalay Resources - Cerro Bayo BALL MILL Open Gearing NDT Record Jan 20
Mandalay Resources - Cerro Bayo BALL MILL Open Gearing NDT Record Jan 20
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Australasian Gearing Services (AGS) were engaged to attend site during the shutdown effected end of
January / beginning February 2015, to assist with the programmed maintenance and overall asset
management of the drive systems of the grinding mills at Cerro Bayo.
Those mobilised to site from Perth, Australia were Wayne Reader (Principal AGS) and Duncan
Butterworth (Principal Weld Integrity).
To carry out a thorough NDT assessment of the SAG and Ball Mill open gearing (Girth Gear /
Pinion) via Magnetic Particle Inspection (MPI).
This was in order to determine:
o soundness of the Girth gears, particularly in Zone #1 (tooth area) the girth gears
o determine current condition of the gearing as a whole
o determine and deem suitability for continued use
o offer recommendations going forward, based upon findings of the assessment
To carry out follow up inspections of gear reducer internals and overlay comparatively with
previous inspection results in November ’14 (when Ball Mill reducer was replaced).
To complete mensuration of the girth gears, measuring and collecting remaining information
that was previously inaccessible during the November ’14 shutdown due to guarding etc
being intact at that time.
Arrival in Chile Chico was in the evening of 29th January where we were collected from the Ferry by
Sebastian Romero and first attendance on site was the morning of 30 th January.
Upon arrival to site the gears weren’t available for commencement of NDT assessment so this was
deferred until 31st January.
Given the delay, this time was utilised to carry out initial inspection of the gear reducer internals of both
the SAG and Ball Mill.
No change in condition was observed to the SAG mill gear reducer however there was deterioration to
the input pinion and bull gear of the previously refurbished ball mill reducer that was replaced, with new
internals in November ’14.
Completion of the mensuration of the girth gears was carried out also during the dwell time prior to
gaining access to the girth gears for NDT assessment.
Access was still unavailable due to issues / problems with the installation of the mill internals so NDT of
the SAG mill gear was again deferred until access was going to be available and final cleaning
completed on 1st February.
Access was gained to the SAG Mill girth gear in the morning of 1st February and completion of the NDT
of the girth gear and pinion was completed during this shift.
Night shift completed cleaning of the gear drive which allowed commencement of the NDT inspection
in the morning of 1st February.
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Upon completion, the gear structure was deemed sound given that no major flaws or cracks were
observed at this time.
However the condition of the current active tooth flanks of both pinion and gear, are such that they can
be considered to have achieved well in excess of their anticipated designed service life and if left
unattended will see further deterioration that will inevitably lead to tooth cracking at the pitch line which
could I turn, expose the gear to potential tooth outbreak.
Other activities were completed throughout the shift also.
Night shift moved the inching drive which allowed commencement of the Ball Mill gearing NDT on 2nd
February.
Once mill rotation via the inching drive was reinstated, completion of cleaning of the girth gear and
pinion was carried out.
NDT of the Ball mill gearing was then eventually commenced and completed with the gear to be found
the girth gear to be sound and in fact, in remarkable condition for the time that it has been in service,
compared to the condition of the SAG mill gear.
The pinion however is suffering due to mismatched profiles and will require eventual replacement but
before any surface degradation is mirrored onto the girth gear.
Contact assessment of the Ball mill gear reducer was attempted however due to not having the correct
medium to utilise (Bearing Blue) to successfully carry out such a check, coupled with the inability to
false load the teeth to derive a reasonable contact pattern, the check was aborted.
Various other activities were completed and a wrap up meeting convened with all relevant parties /
stakeholders from Mandalay Resources, AGS and Mestranza Diesel in attendance.
Discussions centred around firstly, our findings of the NDT assessments of the SAG and Ball mill girth
gears and pinions and associated causes for current condition of each of the gear drives.
In addition, proposed recommendations were outlined and suggested for both machines’ ongoing
operation.
Sebastian assisted greatly with translation during the discussion.
Much emphasis was placed on the findings relating to the internals of the Ball Mill gear reducer and
associated damage that has occurred after only two months of operation.
The root cause for the damage observed appears to be consistent with adverse loading to the output
end of the gear mesh and will be discussed further in the body of the report.
Meeting closed just prior to 18.00 and we travelled back to Chile Chico via the company bus.
An informal dinner meeting was held when Toni arrived in Chile Chico where we had a further
discussion regarding our findings over the course of the shutdown.
We were collected at 7.30 by Marcelo who ensured that we made it to the Ferry on time to commence
our journey back to Perth, Australia.
Wayne Reader
Australasian Gearing Services
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A magnetic particle examination was carried out to 100% of the gear teeth surface areas:
Girth Gear Teeth (287 Teeth)
Pinion Gear Teeth (23 Teeth)
Results of Inspection:
Girth Gear
Uniform contact surface conditions were observed to each tooth through the full circumference of the
Girth Gear, very little damage was observed.
NSD - No Significant Discontinuities has predominantly been utilised to categorise the damage due
to the consistency of the contact surface conditions of the girth gear teeth.
A number of teeth were noted to have been subjected to impact and entrapment of foreign material
resulting in peening at the lands of teeth Nos: #113 & #262, & #287 as well as few contact surface
anomalies.
One particular area centre of face has been subjected to one piece of foreign material (approx. 8mm
in dia) being entrapped and passed through mesh, having affected each of the teeth on both
members.
Refer to pages #4 - #21 for detailed results.
Pinion
Pinion surface conditions and inspection results were consistent with the findings of the Girth
inspection results.
Fatigued material was evident at the DE of each of the pinion teeth with the formation of pitting at the
pitch line.
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TABLE 1 Girth Gear
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TABLE 1 Girth Gear
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Legend: CD - Contact Damage. MiP - Micro Pitting. MaP - Macro Pitting. SS - Sporadic Spalling.
KC – Crack Formation. PLC – Pitch Line Cracking. MiS – Micro Shrinkage. MaS – Macro Shrinkage.
GA – Gasseous Inclusion.NGA – Non Gasseous Inclusion. MML - Minor Material Loss.
AW – Abrasive Wear. RA - Relieved Area. LD – Linea Discontinuity.
NSD - No Significant Discontinuities
Photo # 1: Impact Damage on the Non Drive End Non Load face corner of Tooth Number 113
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Photo # 2: Impact Damage on the Centre Non Load face of Tooth Number 262
Photo # 3: Impact Damage on the Drive End Non Load face of Tooth Number 262
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Photo # 4: Impact Damage on the Drive End Load face of Tooth Number 287
Photo # 5: General view of MPI background being applied to the girth gear teeth
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TABLE 2 Pinion
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During the course of inspecting the pinion and girth gear the following observations were made
relative to the condition of the two members:
Pinion
It was reported that the pinion currently in service was installed in an as new condition and
married with the previously utilised girth gear contact flank, approximately 18 months prior to this
inspection.
Although there are some early signs of deterioration with fatigue due to specific overload,
predominantly at the drive end of the pinion as well as some abrasive wear taking place, in
general, the pinion is in reasonable condition.
However, considering the short period of time that the pinion has operated, coupled with the
current (good) condition of the girth gear, there should be a mechanism put in place to arrest
further deterioration so as to maximise the remaining service life of the pinion.
Not unlike the situation with the SAG mill, part of the reason some of the deterioration can be
attributed to attempting to match two members where one has already been previously utilised
but the majority of the issues with this drive lay with the lubrication, ingress of fine abrasives but
also some mechanical misalignment having been in play at some stage.
The main modes of damage observed with this drive that would be detrimental to successful long
term operation are characterised as follows:
Abrasive wear (three body abrasion) due to the introduction of abrasive contaminants and
wear debris into mesh.
Pitch line overload and fatigue with the early development of pitch line pitting at the drive
end of the face width.
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Enhanced view of DE pinion depicting longitudinal misalignment between pinion and gear
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Enhanced view of DE pinion depicting longitudinal misalignment between pinion and gear
Girth Gear
The Girth gear has been in service since the mine’s inception at Cerro Bayo.
In fact, this is the first time since initial operation commenced that the gearing has been stripped
of lubricant and the condition assessed in any form.
Until the pinion that is currently in service was installed approximately 18 months ago, the original
pinion operated with the original active flanks.
As discussed whilst on site, given the duration of time that the gear has been in operation and
even after being coupled with a new replacement pinion some 18 months ago, the girth gear is in
remarkable condition with little damage, all things considered, with the tooth profile remaining
intact (something almost unheard of).
As the gear is in such good condition, the rate of decline of the pinion appears relatively slow and
has been restricted as mentioned previously, to some pitting starting to occur at the DE of the
face width (due primarily to an overload condition that must have been in play previously and
appears now to have been rectified).
As well as this, some abrasive wear has occurred during normal operation due to ingress of fine
contaminants and as a consequence, an edge and root wear step is starting to develop, which
ultimately will see the vibration levels start to increase over time if left unattended.
Given this I would suggest that the gear drive in its current state (particularly now that it has been
cleared of residual lubricant and likewise any abrasive particulate matter that may have been
harboured in said lubricant), would be suitable for continued use with long term service potential
after a small amount of rectification.
This will be discussed further in the report.
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General view of girth gear contact surface conditions. Note machining witness still visible.
Enhanced view NDE depicting evidence of a slight pitch line overload toward the rim face
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Enhanced view DE depicting evidence of a slight pitch line overload toward the rim face
General view of area of damage to #262 presumed to have occurred during pinion installation
This damage was relieved during the course of the shut down
Gear Mesh
As mentioned previously, the Girth gear has been in service since the mine’s inception at Cerro
Bayo with one pinion replacement carried out approximately 18 months ago.
Although we have not witnessed firsthand, the condition of the pinion that was removed, I’m
assuming that it was also in reasonable condition when replaced.
As mentioned previously, I would like to take a look at any photographs of the previously utilised
pinion if they are readily available.
The current contact and load distribution between the two meshing members appears reasonable
and the values measured below indicate that alignment conditions are good.
If there are any (most recent) dynamic results (infra red readings) available, if I could be furnished
with a copy that would be greatly appreciated so that I can look at dynamic vs static
comparatively
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Gear Reducer
A post installation follow up inspection of the gear reducer was carried out, so as to assess first
and foremost, the condition of the replacement internals that were installed in November ’14, after
two months operation.
Initial inspection of the externals and seal carrier peripherals deemed that the seals all remain
intact with no leaks observed.
The breather was noted to be in good condition and had not reached expiry so was deemed
suitable for continued use.
The inspection hatch was then removed to gain access to the internals and an immediate flag
was raised due to some unexpected damage being noted at the output end of the active flanks of
the input pinion, as well as corresponding damage to the active flanks of the output (bull) gear.
Closer investigation of the defect (as best as is available via the access hatch) was made and the
damage categorised as either early stages of destructive pitting or potentially, localised case
crushing.
Further and even closer examination would be required to absolutely define the exact mechanism
of failure that is occuring however under either scenario, these type of failures occur when the
basic fatigue load capacity of the material has been exceeded, either due to application of too
much torque or poor load distribution along the tooth or between several pairs of teeth.
In this instance, given the adverse loading to the output end of both members and the strange
longitudinal contact (as depicted through the lead angle on the bull gear teeth), this will almost
certainly be the major contributing factor to the failure mechanism being seen.
Further enhanced view of active flanks of input shaft – note area of overload
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General view of active flanks of output shaft – note odd longitudinal contact and area of overload
Further enhanced view of active flanks of output shaft – note area of overload
General view of gear reducer depicting clean seal carriers (void of oil leaks)
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To recap on our findings, we have determined during the course of these inspections, the
following:
The mill and associated gear drive system has been in operation for the last 20 years
(approx.) since installation in 1995.
Having had no exposure to the drives at Cerro Bayo until August 2014, our comments
and recommendations can only be at best, from that period onward.
The gear had operated with the original pinion until approximately 18 months ago. The
exact reasoning behind the replacement is a little grey at this point due to the gear being
in as good a condition as it currently is (some photographs of the previously utilised
contact flanks would be useful).
There are a few surface anomalies that require attention so as to arrest any further
degradation as outlined previously.
The same open gear lubrication, associated delivery system and operating philosophy
has been utilised since the commissioning of the mill and to date, appears to have
served the machine well.
The active flanks of the girth gear are in remarkable condition for the time that the mill
has been in service and if looked after and remain incident free, should serve well for a
number of years to come.
Zone #1 of the gear structure was NDT assessed and at the time of assessment, was
deemed to be sound from an MPI inspection perspective (no detrimental surface
discontinuities were uncovered).
The inactive flank is unused and was found to be in an “as new” condition.
We have determined that the girth gear is sound and suitable for continued use however so as to
ensure or retard the potential of any further degradation, we would highly recommend some
remedial work be carried out to the pinion to relieve any fatigued material that would eventually
lead to progressive pitting and spalling.
It is also recommended that any remedial work be carried out only by an experienced gear
specialist.
If you so desired, we could assist in this area but would provide specific particulars under a
separate cover to this report.
We have determined the SAG mill pinions are symmetrical therefore we also require that the
same clarification be made for the ball mill pinions.
Should they not be symmetrical, there will need to be another replacement pinion manufactured
given that there is no spare available at present.
Please note: as you have no other new spare pinion, if the pinions are in fact not reversible,
Cerro Bayo’s “exposure to risk” profile alters / increases considerably.
Should there be some sort of pinion failure experienced now, we would have to resort to
reinstalling the previously utilised pinion, at least in the short term.
Not knowing the current condition could also present a problem so this also needs to be
ascertained.
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Also during our wrap up meeting, the question was posed as to whether I thought the lubricant /
lubrication of the drives is suitable.
This is quite a subjective area and I would prefer this left for the most part, to an alternate forum.
However, I will say that although there are more technologically upmarket lubricants and
dispensing systems available in the market place today, consideration needs to be offered to the
fact that the drives at Cerro Bayo have been operating on the current lubricant and associated
equipment since 1995.
Gear Reducer
The overall history surrounding the grinding mill gear reducers at Cerro Bayo remains somewhat
clouded.
During the course of the shutdown in November ‘14, whilst the newly refurbished gear reducer
was being replaced, the soleplates were manually checked for flatness and identified as not being
flat and true (potentially in both planes).
As previously reported, rudimentary assessment was made with a straight edge longitudinally
(parallel to the mill operational centreline) and perpendicular to the rotating members of the
reducer.
The soleplates were found to be notably lower in elevation toward the centreline of the gear
reducer, with the outer extremities obviously higher.
The inboard gap previously measured was in excess of 0.4mm on the inboard side of both
soleplates, which equates to a significant discrepancy across the width of the gear reducer
(coupling face to coupling face – particularly considering the additional output shaft extension).
We have been led to believe by MD personnel during the course of the wrap up meeting that
when the reducer was refurbished in Concepcion, the underside of the case was milled flat and
utilised as a datum (as is typical in new reducer manufacture and refurbishment alike) to the rest
of the re machining tasks that were carried out.
Although there has been no dimensional documentation (MDR / Rebuild report) that has been
made available to support this to date, there were some photographs circulated in a document
that confirmed adequate tooth contact post rebuild (presumably in a relaxed condition).
Given that this is a single reduction parallel reducer, coupled with the fact that the mesh was
confirmed as being acceptable after reassembly at MD (again, presumed in a relaxed condition
with new input and output gears), there clearly have to be other factors that are contributing to the
misalignment of the two members whilst the gear reducer is in operation while the soleplates are
known to be an issue.
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So, if we can rely on the verbal affirmation as being correct, that the datum was established first
and then the rest of the re machining was carried out after this, we can be sure this would
certainly offer a best case scenario toward the best possible outcome as far as the gear reducer
installation is concerned
However when torqued down, the likelihood of a bend or twist being induced into the gear case is
extremely high and not something that can be readily improved by shimming the underside of the
gear reducer landing pads, due to the soleplate irregularities.
Inducing such stresses and resultant twist across the gear case is really the only way that this
mesh could see a misaligned condition and subsequent localised overload to one end of the gear
set, such as we have seen occur with this installation.
Knowing that we have a flatness / trueness issue, there are two potential scenarios that need to
be given consideration to alleviate the problem at hand, otherwise we will continue to see
repeated reducer failures going forward.
At this point in time we believe that the best course of action is to consider option #2 given that it
will be quicker and far less expensive than supply and total replacement of the soleplate even
before we consider the extended down time that would be involved to effect option #1.
There is a requirement to rectify the problem sooner than later and the following should be
considered as a minimum going forward, at least until all issues are resolved:
If there is an unplanned shutdown experienced, the gear reducer inspection hatch
should be opened and the internals photographed and forwarded to us for immediate
assessment to determine if there is any further degradation taking place.
At a minimum, a quick shut should be planned for a monthly check if possible.
Have the refurbished reducer shipped immediately to Cerro Bayo from MD (assuming it
has been completed) so that it is available for immediate replacement if required.
Plan at a minimum to have a quarterly (or in line with scheduled maintenance outages)
inspection carried out relative to the open gears as well as the reducers
Commence planning with MD (or others) relative to supply of personnel and equipment
to effect the suggested in situ machining at our earliest and most practical opportunity
We can work in tandem or head up any potential rectification works if you so desire us
to do so.
Procure a second spare gear reducer
As requested by site personnel, I have also obtained a quotation for a drop in replacement
gear reducer from FALK Australia.
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Conclusion
I believe that we have covered the majority of the tasks that we set out to achieve over the course
of the shutdown and look forward to your response to our submission.
If there are any questions, anything that you may feel that I have missed or anything that we can
be of further assistance with, please don’t hesitate to contact myself at your earliest convenience.
Best regards
Wayne Reader
Australasian Gearing Services
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