Spark Errossion
Spark Errossion
PrimeServ Copenhagen
REPORT
Name of Vessel: M.S. Energy Conqueror IMO No: 9275660
Engine Type: 6S60MC-C Sea Trial: 2003-12-17
Engine Builder: STX Engine No: SB3055
Job Order No: 40023749 Run. hours: 37700
Visit by: Peter M. Christensen and: Service Center: Copenhagen
- Niels Fischer Semdahl
- Kim Nothlev Larsen
- Arne Kvistgaard Petersen
- Steen Cosmus Thaning
- Henrik W. Christensen
- Flemming Olsen
Spare parts from MAN: Yes No X Spare Order No: -
External Workforce: Yes No X Workshop: -
Place: Greece/Perama ECS Version: -
Period: 2011.01.14 – 2011.03.30 (including travel)
Owner: Enterprises Shipping & Trading
Requested by:
Reason: Main bearing #1 failure.
Keywords: Main bearing, spark erosion, shaft earthing, in situ machining
2011-04-11
PEMC/CLL
BACKGROUND
On December 24th an oil mist indicated problems surrounding cylinder unit #1.
The vessel with cargo was towed to anchorage off Malta.
Investigations performed by MAN Diesel & Turbo (MDT) concluded that main bearing #1
was severely damaged from overheating and that main and thrust bearings had suffered
from spark erosion as a result of a faulty shaft earthing system. During the preliminary
inspections, other possible root causes were carefully eliminated one by one based on
findings.
The cargo was discharged and the vessel was towed to Greece/Piraeus.
MDT attended and the repair commenced. The owner agreed to carry out an in situ
machining of the crankshaft journal and bearing support, without lifting the crankshaft from
its position.
The bearing support #1 was verified to have collapsed and the vertical and horizontal
surfaces were deformed as a result of this.
The vertical and horizontal landing surfaces were filed and polished by hand until an
acceptable contact was established using a template and blue marking.
The bearing support was machined by in situ machining and the final diameter was plus 0.3
mm.
PrimeServ Copenhagen
3/4
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
The bearing cap was also verified to have collapsed and the vertical and horizontal landing
surfaces were machined to adapt to the new geometry of the bearing support. The new
bearing cap geometry was established in a workshop.
A new bearing shell was manufactured and tailored to the established bearing geometry.
It is recommended to open the bearing for inspection within 2 months and thus verify the
load pattern. This operation must be supervised by a MDT specialist. It is recommended to
install the spare bearing during this operation in order to verify its crush and adapted design.
CHAIN DRIVE
The two chains had each an assembly point. Visual inspections revealed that these two
outer links were not assembled properly as the mating surface of the pins did not touch the
lash. When the flywheel was at 105° the links were not in a position for dismantling and two
other links were identified to be opened.
The chain was opened, and the free ends lowered to the sump. Chain blocks were used to
secure the camshaft wheel, pull each free end down, and to free the lower gear from the
chain. On completion of the bearing repair, a set of new outer links were installed, the chain
was tightened and the timing checked of camshaft and starting air distributor.
Then the two faulty chain links were removed and replaced by new. It was revealed that one
of the pins could be inserted by hand into the lash. This is supposed to be a very tight fit.
The holes had been made larger during the original assembly.
It is recommended to monitor the 4 new chain links and make inspections after 24, 200, 500,
2000, 4000 running hours.
The rubber guide bars were found defective and replaced by new.
THRUST BEARING
Please refer to appendix: #11, 12, 13
The clearance of the assembled thrust bearing was 0.16 mm. The nominal clearance is
above 0,50 mm. The thrust collar was full of adhered white metal as a result of spark
erosion. The segments in AHEAD direction were in average worn to 95.73. The nominal is
95.98-96.00 mm from new. During service the segments may wear to 95.01 mm. The
surface was in a very bad condition, and the high spots have ruined the oil film and
contributed to the low clearance measured. The white metal was replaced on all segments.
It is concluded that the thrust bearing was damaged as a consequence of spark erosion.
FLUSHING
Please refer to appendix: #14
The engine was flushed for 75 hours, bypassing the bearings, chain drive and camshaft, and
then another 115 hours of flushing including the lower chain drive and subsequently the
remaining bearings. Oil sample was sent to Mobil for analysis according to ISO4406
XX/19/15 after 24 hours of flushing. However, the received analyse result did not comply as
there is no particle counting included.
DISMANTLING AND ASSEMBLING OF INTERMEDIATE SHAFT
Please refer to appendix: #15
PrimeServ Copenhagen
4/4
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
MDT was not involved in this task. We recommended pulling the fitted bolts rather than
pushing towards the crankshaft. A contractor carried out tag welding on the crank shaft
during his machining of the holes for the fitted bolts at the flange between crankshaft and
intermediate shaft. MDT urged to abandon the welding, suggested an alternative method for
keeping the milling machine in position, and made a repair procedure for the welded areas.
ENGINE TEST
Please refer to appendix: #16, 17, 18
The function of the oil mist detecting system was verified by a contractor prior to starting the
engine.
The engine was tested in accordance with the agreed program, and the bearing #1 was
found in an acceptable condition. MDT will produce the spare bearing in accordance with the
findings.
INDEX OF APPENDIX
Appendix 01 - determining the geometry of saddle and bearing cap #1
Appendix 02 - determining the geometry of bearing cap #1
Appendix 03 - inspection of crossheads
Appendix 04 - inspection of main bearing journals
Appendix 05 - inspection of main bearing shells
Appendix 06 - fitting of new bearing shell
Appendix 07 - bearing cap landings – x-y off malta
Appendix 08 - deflection in preparation to main bearing #1 support machining
Appendix 09 - bearing cap landings - type of damage
Appendix 10 - journals and pins after repair
Appendix 11 - inspection of thrust collars
Appendix 12 - inspection of thrust segments
Appendix 13 - specification of babbit
Appendix 14 - flushing
Appendix 15 - inspection crank shaft flange flywheel end
Appendix 16 - dismantling and assembling of intermediate shaft
Appendix 17 - oil mist detector report
Appendix 18 - engine test
Appendix 19 - crankshaft damage - root cause
Appendix 20 - sl2008-498
PEMC/CLL
2011-04-11
PrimeServ Copenhagen
1/1
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
The cap bore and mating surfaces were mapped by means of a 3D measuring
device and the results are listed below.
Unit # 3 Unit # 5
Aft Shoe, cam side Aft Shoe, cam side
This surface is white metal lined. The bearing material has been
exposed to a local overload as a
result of a protruding corner of a
misaligned bearing shell.
Cam side aft Exh side aft Cam side aft Exh side aft
Recommendation:
1. Replace x-head shoe #3 and #5 aft.
2. Ensure 1 mm clearance at the end of the bearing shell during assembling
3. Remove any high spots on bearing shells as a result of stamped in
numbers
4. Remove any high areas on the other crosshead shoes in the vicinity of
the shell edge.
Item 2, 3 & 4 were done during assembling. Item 1 can be done during the next
dry dock. Crew to monitor the crosshead shoe bearing, i.a. by looking for debris
in the crank case compartment and the lubrication oil backflush filter.
PrimeServ Copenhagen
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M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Areas with Sn
adhered to the
journal due to
Spark erosion
PrimeServ Copenhagen
2/3
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Check the clearance between upper shell and bearing cap and lower shell and
bearing support at full perimeter by 0.05 mm Kjær Feeler. Result – no
clearance.
PrimeServ Copenhagen
3/10
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Blue ink on upper and lower shell outer side. Pressure 700 bar.
Upper Lower
Blue ink on upper and lower shell end surface. Pressure 700 bar.
CAM EXH
PrimeServ Copenhagen
4/10
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Blue marking on upper and lower shell outer side. Pressure 1500 bar.
Upper Lower
Blue ink on upper and lower shell end surface. Pressure 1500 bar.
Blue ink on vertical and horizontal mating surface of cap. Pressure 1500 bar.
CAM EXH
Lower bearing shell load picture after 720° turning @90° flywheel angle.
With blue After cleaning
PrimeServ Copenhagen
5/10
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Journal with blue ink after 720° turning @90° flywheel angle. Pressure 1500
bar.
At 1500 bar the bearing clearance was measured with below result:
Neck of the web is used as measuring point while turning with reference to
flywheel angle.
Flywheel angle [°] TDC 15 30 45 60 75
1
Forward / 100 mm - - - - - -
1
Aft / 100 mm 5 0 5 15 15 20
Flywheel angle [°] 90 105 120 135 150 165
1
Forward / 100 mm - - - - 25 30
1
Aft / 100 mm 30 20 30 25 25 30
Flywheel angle [°] 180 195 210 225 240 255
1
Forward / 100 mm 45 50 35 - - -
1
Aft / 100 mm 40 45 35 35 35 35
Flywheel angle [°] 270 285 300 315 330 345
1
Forward / 100 mm - - - - - -
1
Aft / 100 mm 35 30 20 15 5 5
Web is located at 90° flywheel angle while measuring the bearing cap:
Reference to TDC [°] -30 -15 TDC +15 +30
1
Forward / 100 mm 25 40 50 45 25
1
Aft / 100 mm 25 40 45 45 25
Deflection measured when temperature of crank shaft was 35°C and engine sump tank was
45°C.
Lower shell
Upper shell
PrimeServ Copenhagen
10/10
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Main bearing journal #2 through 8 have been polished and the original topography has been
established without altering the journal geometry. The geometry was verified by blue
marking and more than the nominal 70% contact was established.
Crank pin bearing journals #1 through 6 were all polished and the nominal 60% contact was
verified by blue marking.
PrimeServ Copenhagen
2/3
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
180° 270°
The following roughness has been measured on completion of the polishing by means of our
instrument:
Make: Time Group
Type: TR110 Surface Roughness Tester
Calibration date: 29.01.2011
The following roughness has been measured on request from DNV by means of our
instrument:
Make: Mahr Gmbh
Type: MarSurf PS1 Surface Roughness Tester
Calibration date: 01.03.2011
The measured values are all fully acceptable for an engine in service. Visible scratches were
observed and they are considered normal and acceptable in view of the actual running hours
of the engine.
PrimeServ Copenhagen
1/2
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
AHEAD and ASTERN thrust collar were found with excessive Sn adhered to
them as a consequence of spark erosion.
Repair proposal: AHEAD collar to be machined using a superfiner. AHEAD and
ASTERN collar to be polished by hand to a roughness less than 0.8 Ra.
1
Flywheel angle. 0° is cylinder #1 in TDC (Top Dead Centre)
PrimeServ Copenhagen
2/2
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
AHEAD and ASTERN bearing segments were found with excessive damage
and wear as a consequence of spark erosion.
Please refer to the next page for measurements Top, Mid and Bottom.
PrimeServ Copenhagen
2/5
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
F5 F6 F7 F8
1
Flywheel angle. 0° is cylinder #1 in TDC (Top Dead Centre)
PrimeServ Copenhagen
3/5
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
A5 A6 A7 A8
1 2 3 4 5 6 7 8
Top 95.99 96.00 96.00 96.00 95.99 96.00 95.65 95.50
Mid 95.98 95.99 95.98 95.98 95.97 95.98 95.71 95.59
Bottom 95.97 95.97 95.89 95.92 95.86 95,86 95.77 95.73
PrimeServ Copenhagen
4/5
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Material eroded.
PrimeServ Copenhagen
5/5
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Certificate of analysis
S11 Balance
Sb 7,55%
Cu 3,24%
Pb 0,075%
Fe 0,042%
Zn 0,003%
As 0,024%
Al 0,001%
Ni 0,212%
Bi 0,025%
Cd 0,891%)
Ag 0,095%
Kim J0rgensen
Appendix 14
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Page 1 of]
SIGNUM
30242053 Normal
Account NumbE,r 12690:3 Date 22-Mar-2011
Account Name Enterprises Shipping & Trading SA Description Main Engine (Before Purifier)
Application MARINE - ENGINE
IMO Number 9275660 Manufacturer MAN/B&WNS
Vessel Name Energy Conqueror Model S60MC
Equipment Number 001 RegisterE~d Lubricant MOBILGARD 300
~;ments: No action is required on oil or enlline. - Results are within acceptable ranges. - Examine progressive changes and monitor results for Changin911
trends. - Sample at next scheduled interval. I,
Results and comments of this analysis are advisor( only; the validity of the data
I
may be impaired by a non-representative sample or incorrect data. This analysis is •
provided for the confidential information of the partv subm~ting ij. Any use by any EJf(onMobli
...
[_N_o_r_m_a_I...I.._+_G,aution 'Alert I other person is prohibited. © Copyright 2003 Exxon Mobil Corporation. Exxon,
Esso, Mobil, ExxonMobil and Signum are trademarks of ExxonMobii Corporation or .
one of its subsidiaries. Marketing Affiliate -
PrimeServ Copenhagen
1/2
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Recommendation: Machine the holes and fit oversize fitted bolts in accordance
with class rules and the necessary calculations.
Appendix 16
Peter Melgaard Christensen
From: Flemming Olsen
Sent: 7. marts 2011 15:21
To: '[email protected]'
Cc: Post-DT-CPH; Peter Melgaard Christensen; Martin Jakobsen
Subject: RE: M/T ENERGY CONQUEROR - Connecting intermediate shaft to crank shaft
Attachments: image001.gif
As outlined it is not acceptable to weld on the crankshaft due to risk for hydrogen cracks and hardening of the
material.
1) The welding should be machined away planar to the flange. The surface should be checked for cracks with
fluorescent magnaflux. For reference the hardness is measured at the welding spot and out in the base
material.
2)
a. If no cracks are found in step 1), the heat affected zone is removed by machining to a depth of 2 mm
(and 3 mm outside of each welding spot). A smooth transition to the surface should be made with a
radius of minimum r=4 mm. To have sufficient contact area for the nut, the grinding should be limited
to the immediate area around the welding.
b. If there are cracks in step 1) the 2 mm are machined of in steps off 0.5 mm (and 3 mm outside of
each welding spot) until crack free zone is reach and from there the remaining (minimum 0.5 mm)
down to total 2 mm is machined off (If more than total 2 mm need to be machined off we should be
contacted first). A smooth transition to the surface should be made in same way as in 2a.
3) Hardness is measured at the welding spot. The surface should be checked for cracks with fluorescent
magnaflux
4) Diagram with the dimension of grindings relative to the bolt hole is made.
Please return with above data for our acceptance of the repair.
Kind regards
Flemming Olsen
Marine & Project Engineer
Large Repairs
1
Phone: +45 33 85 11 00
Direct: +45 33 85 28 73
Mob: +45 24 66 48 17
[email protected]
[email protected]
www.mandieselturbo.com
Kindly note that MAN DIESEL TURBO can not accept welding on crankshaft.
We kindly ask you to take contact to local Superintendent and inform him accordingly.
We will return with our suggestions to save the crankshaft later today.
Kind regards
Flemming Olsen
Large Repairs
2
Phone: +45 33 85 11 00
Direct: +45 33 85 28 73
Mob: +45 24 66 48 17
[email protected]
[email protected]
www.mandieselturbo.com
3
Appendix 17
PrimeServ Copenhagen
1/3
M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
Unit 1 2 3 4 5 6
FWD/AFT FWD/AFT FWD/AFT FWD/AFT FWD/AFT FWD/AFT
CAM top 0/0 0/0 0/0 0/0 0/0 0/0
FWD bottom 0/0 3/3 5/5 0/0 5/5 0/0
EXH top 35/35 35/35 30/30 25/25 30/35 30/45
X-head shoe FWD bottom 25/25 40/40 40/40 45/45 40/45 40/45
CAM top 0/0 0/0 0/0 0/0 0/0 0/0
AFT bottom 0/0 0/0 0/0 0/0 0/0 0/0
EXH top 20/20 30/35 25/25 25/25 25/25 30/30
AFT bottom 45/40 40/40 40/40 45/45 35/35 35/40
Engine was started and operated for 5 hours at 100% rpm. A set of indicator diagrams were
taken.
Main bearing #1-8 Guide plans unit #1- Crankpin #1-6 X-head #1-6
6
44°C 48/58°C 44°C 44°C
PrimeServ Copenhagen
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M.T. ENERGY CONQUEROR IMO No. 9275660
6S60MC-C Engine No. SB3055 Run. hours 37700
2. Bearing #1 was opened for inspection – it was not deemed necessary to scrape the
bearing as the load pattern appeared as expected.
3. Checking lube oil outlets from crossheads - OK
4. Scavenging port inspection – carried out by crew
Closing remark:
A crankshaft deflection was carried out after loading the vessel with cargo at first loading
port. This deflection is listed below:.
Dear Mr D.Drobonis,
With reference to your e-mail dated 8.March 2011 regarding damage to crankshaft main journal 1 and the bearing
saddle we have the following comments.
There are the following four reasons for bearing failure in a two stroke engine of our design.
1) Human error.
If, after an inspection, the bearing has not been correctly assembled which means that the bearing shells
have not been positioned according to the instructions given in the instruction book, Volume
II.
Such a mistake will cause bearing failure after few hours of running. We have not received any information
from your representatives onboard that bearing No.1 was inspected shortly before the bearing damage, so this
must be excluded as a root cause for this damage.
In case the crankshaft journals from when they are new exceed our specifications for ovality, conicity,
diameter and roughness or the bearing saddle/bearing cap should deviate from the given design, it is our
experience that breakdown of the component in question will occur in a period of the first 0-3000 hours after
the engine is put in operation and it is the same for possible fatigue of the bearing material. Due to the fact
that the vessel was delivered in 2004, and without any reported problems during the garantee period, this
reason for the bearing failure can be eliminated.
1
A commonly occuring reason which causes damage to the journal surfaces and the bearing material is the
contents of particles in the lub.oil with a size bigger than acceptable according to MAN Diesel & Turbo’s
specification which is an absolute filter fineness of maximum 50 micron.
There can be many reasons for contamination of the lub.oil. The most common one is sludge from the
scavenge air boxes falling into the crankshaft housing during piston overhaul, or sandblasting material
entering into the engine room during dry docking. However, a properly working filter will trap these impurities
before the oil enters into the bearings. In case the lub.oil filter elements are damaged or missing the
impurities will be carried by the lub. oil into the engine, and the risk for bearing failure is then present. The first
indication of particle contamination of the lub. oil is round going scratches on the crankshaft journals and
scratches on the cross pins and imbedded particles in the bearing material.
We have not found any indication of contaminated lub. oil onboard M/V Energy Conqueror. All journals were
found without any scratches, the surface roughness was measured on all cross pins with an electronic gauge
and found in order (surface roughness less than Ra 0.09). There has not been found any bearing shells (main
bearing, crankshaft bearing or crosshead bearing) with embetted particles. As no indications of particle
contamination of the lub.oil were found, we can acquit the lub.oil as root of the failure of main bearing No.1.
4) Spark erosion.
Spark erosion can occur if electrical potential in the crankshaft discharges through the main or thrust bearings
instead of via the earthing device mounted on the propeller shaft.
Please find attached our ServiceLetter SL08 – 2008/498/AAB which describes, on pages 3-4-5, bearing
damage caused by spark erosion. Please compare the photos shown in the service letter with the photos
below taken onboard M/V Energy Conqueror.
Ahead side of the thrust collar was found with excessive Sn adhered to the surface as a consequence of
spark erosion.
2
On all main journals clear sign of spark erosion was found. Below some examples of the main journal surface.
Journal 5
As can be seen on the above photos it is evident that the bearings and thrust segments have been exposed
to severe spark erosion.
As mentioned in your mail several bearings were opened up during the vessel’s dry docking March 2009 for
class survey and no signs of spark erosion was observed.
It requires a ”trained eye“ to spot spark erosion in its early stage, so it is understandable if the DNV inspector
overlooked signs of spark erosion, in case the erosion had started at that time.
It is not possible to predict a precise time frame from erosion begins and to the a severe damage takes place,
but we have experienced that insufficient earthing of the crankshaft and propeller arrangement are able to
generate deterioration of the bearing material in less than six months with severe damage as a result.
Hope the above explanation has answered your questions regarding the damage to main bearing No.1
3
Kind regards
Niels Semdahl
Superintendent Engineer
Phone: +45 33 85 11 00
Direct: +45 33 85 15 71
Mob: +45 21 43 79 45
[email protected]
[email protected]
www.mandieselturbo.com
4
Appendix 20
Concerns
Owners and operators of all MAN B&W
two-stroke marine diesel engines.
Contents
Dear Sirs About Spark Erosion page 2
Shaftline Earthing Device,
This is an update on spark erosion, and how to discover and prevent it. installation & maintenance page 2
Spark erosion can occur if electrical potential in the crankshaft discharg- Discover Spark Erosion page 3
es through the main or thrust bearings. If undiscovered, spark erosion Incorrect Installation page 6
can cause critical wear on the main bearings, and consequently severe Insufficient Maintenance page 7
crank train damage.
Spec. No. 0792182-1 Appendix
From practical experience and testing, we know that the best protection
against spark erosion is to use a correctly installed and well-maintained
shaftline earthing device.
Therefore, MAN Diesel now recommends all MAN B&W two-stroke en-
gine operators to:
• Equip all newly ordered engines with a shaftline earthing device with
specifications according to MAN Diesel specification No.Propeller
0792182-1.
Shaftline
• Equip all engines in operation without a shaft monitoring system with Earthing Device
such a shaftline earthing device.
• Inspect and evaluate all existing shaft monitoring systems on engines
V
in operation. Update and overhaul if necessary.
Please direct any questions about this service letter to our Operation
Department: [email protected]
Yours faithfully
Propeller Shaft mounted Current Thrust Main bearings
shaft alternator bearing
Head office (& postal address) PrimeServ Production Forwarding & Receiving MAN Diesel A/S
MAN Diesel A/S Teglholmsgade 41 Teglholmsgade 35 Teglholmsgade 35 Denmark
Teglholmsgade 41 2450 Copenhagen SV 2450 Copenhagen SV 2450 Copenhagen SV Reg. No. 39661314
2450 Copenhagen SV Denmark Denmark Denmark
Denmark Phone: +45 33 85 11 00 Phone: +45 33 85 11 00 Phone: +45 33 85 11 00
Phone: +45 33 85 11 00 Fax: +45 33 85 10 49 Fax: +45 33 85 10 17 Fax: +45 33 85 10 16
Fax: +45 33 85 10 30 [email protected] [email protected]
[email protected]
www.mandiesel.com MAN Diesel – a member of the MAN Group
Service Letter SL08-498/AAB
Monitoring
equipment Corrosion between the slip ring and the shaft can be difficult
Cable connected
with mV-meter to the hull to detect. We recommend these procedures:
• No monitoring voltmeter installed:
Cable to
Slip ring
alarm system
Measure electrical contact between slip ring and shaft at
Slip ring for
least monthly to reveal any concealed corrosion.
monitoring Brush holder If resistance exceeds 5 mΩ: Overhaul the slip ring.
equipment arrangement
• Monitoring voltmeter installed:
Shaftline earthing device parts Check shaftline earthing device monitoring monthly.
AlSn40 Lining
This is a journal, main bearings and thrust collar with clear
signs of spark erosion. Spark erosion signs are obvious,
even in the upper main bearing shell.
AlSn40 type main bearing and journal. Indications of Spark erosion even in the upper
shell.
Corresponding main bearing lower shell with wide spread journal imprint.
0.5 mm of the shell is worn off between the two distinct, visible lines.
This bearing can be re-used after dressing up. The journal When inspecting the thrust collar surface or the main bear-
must be polished to meet surface roughness specifications. ing journal, remember:
Slowly turn the engine 360˚/1 revolution, and inspect the en-
tire surface very carefully.
Note:
• Install a silver covered slip ring between the brushes and
the shaft to ensure sufficient electrical contact
• Replace the slip ring before the silver layer is worn
through.
• Inspect brushes regularly, and re-adjust brushes when
necessary. Poor hardware quality
Fig 1.adjusted
Poorly – Overhaul
brushesand inspections
Note:
• Inspect the brushes if the voltmeter reads more than
50 mV.
• Re-adjust the brushes if they have insufficient contact
with the slip ring. Corrosion hiding behind the slip ring
Note:
ALWAYS polish the propeller shaft carefully and apply rust
protection (e.g. Dinitrol 300) between the Ag band and the
shaft when assembling and overhauling.