3. Energy Tech
3. Energy Tech
Hyderabad
23rd May 2024
Enhance. Enrich.
Net Heat Rate Reduction Concept - CPP
• Net Heat Rate [NHR] = Gross Heat Rate [GHR] / [100 – APC]/ 100]
Enhance. Enrich.
Orient Paper Mills –Amlai is presently having HP Cogeneration Plants in Operation
1 No. 150 TPH AFBC Coal fired Boiler [ Steam Pressure /Temperature: 87 ksc/
510ºC] AFBC Boiler with Feed water temperature at 190ºC connected to 30MW
Multi-extraction [ MHP, LP, LLP] Condensing [ Water cooled condenser] Steam
Turbo-Generator.
Enhance. Enrich.
AFBCB & CRB HP COGEN BATTERY IN OPM
HPS HPS
• . ~G
• . STG ~G
STG
MP 25 MW
MP 30 MW
LP
LP EXH
EXH
C
C
Spray Pond
Enhance. Enrich.
INNOVATIVE ECS # 1 FOR NHR REDUCTION
Enhance. Enrich.
CW Pumps Power Optimization with Both Extraction Condensing STGs in operation
Constant Cooling water flow rate designed for Rated Condensation ( max.) flow is
being maintained all along –irrespective of exhaust steam condensing flows.
Cooling water Pump(s) hence are designed for maximum condensing flows with
design margin on flow & head necessitating constant high auxiliary Power
Consumption at all [Low/Medium /High] Condensing loads of operation.
Innovative energy scheme had been developed for adjusting cooling water loads to
suit varied condensing flows . Hence it was proposed to reduce the circulating
cooling water load to condenser at lower condensing loads to suit. This has in
principle approval & acceptance of Siemens.
Hence cooling water flow to condensers shall be lowered at lowered condensing
loads for effecting reduction in MCW Pump power consumption [APC].
Enhance. Enrich.
High APC of CW Pumps in [Extraction] Condensing STG Battery
- Exhaust Steam Condensing Flows are being split between the 2 Steam Turbines
- Invariably in Cogen units, Extraction steam for process is very high with
balance only for condensing steam
- APC Very High at 1.05 MW with 2 CW pumps in operation even with Condensing
flows < 50 % of rated value.
- Moreover, the CW Pumps had been designed for 1.3 times Design load.
Enhance. Enrich.
CW Pumps Optimization with Both Extraction Condensing STGs in operation
EARLIER
2 CW pumps of very high flow rate [5300 m3/h each] had been in operation all
along. As the requirement of CW flows for the 2 Condensers are far less [~3800
m3/h] even at rated high condensing loads of 57 to 64 TPH, Power consumption is
uniformly high at around 1.0 to 1.1 MW.
It was decided to put in practice the innovative concept of varying the cooling
water flow to condenser as under :
As the condensing loads in each of the turbines are very low viz., 25 to 30 TPH, it
had been decided to operate 1 CW pump catering water flows to both the
condensers.[ As & when the condensing loads go up > 30/35 TPH on a sustained
period, both the CW pumps need to be operated].
Enhance. Enrich.
REDUCTION IN APC WITH 1 of 2 MCW PUMPS OFF
25000 24050
20000
15000
12678
11512 11522 11378 11476
10000
5000
0
Aug-23 Nov Dec Jan-24 Feb Mar
2 Pumps on 1 MCW Pump on
Enhance. Enrich.
Innovative Concept of Varying Cooling water flow with Condensing Loads
• New Energy Efficient lower duty CW pumps [200 kW] one with Fixed
speed & the other with Varying speed alongwith IE3/IE4 motors. The
proposed cooling water pump shall be with VFD so as to vary the
cooling water flow to condenser to suit the varying condensing steam
flows. Through this process, APC from CW pump(s) shall be lowered-
resulting in increase in net power available for process.
• Though Cooling water flow through the condenser tubes had been
designed for exhaust steam condensation rated capacity, the CW flow
rate shall be reduced suitably with lowered condensing loads with
Varying speed of the 2nd CW pump in operation.
• APC is expected to be reduced further by 100 to 150 kW
• Net Heat rate reduction is ensured.
Enhance. Enrich.
ENERGY GAINS & DECARBONIZATION
APC reduction & Net Heat Rate Improvement
Existing [Planned]
Enhance. Enrich.
MULTI-EXTRACTION CONDENSING STG
30 MW ES DF MONITORING
STG
HPS
~G
STG
• . .
MP
LP C
EXH
Enhance. Enrich.
HEAT RATE & CYCLE EFFICIENCY– 30 MW STG - ILLUSTRATION
Enhance. Enrich.
STEAM TURBINE EXTRACTION/EXHAUST ON HEAT RATE
30MW STG Multi-stage Extraction -Exhaust steam condensation with Cooling water
35
32
30
Power Conversion [%]
25 23
20 18
15
15
10 9
0
Extraction / Exhaust Stage of 30 MW Steam Turbine
HPE MP LP LPH C
Enhance. Enrich.
INNOVATIVE METHODOLOGY FOR SUSTAINED HEAT RATE IMPROVEMENT
• Turbine exhaust steam flow, Vacuum, Cooling water flow rate alongwith
inlet & outlet temperatures to 30 MW STG Condenser shall be measured
with on-line temperature sensors on line & transferred to DCS for
continuous recording.
• With all of the above in place, turbine exhaust steam enthalpy shall be
computed [ with the developed Innovative Algorithm ].
Enhance. Enrich.
INNOVATIVE METHODOLOGY FOR SUSTAINED HEAT RATE IMPROVEMENT
Enhance. Enrich.
INNOVATIVE ECS # 2 FOR NHR REDUCTION
Enhance. Enrich.
STG Condenser Lukewarm Cw return for preheating DM Water
LP Steam
CFB
Deaerator
PHE 1
CW Ret-
DMW DM
Water
Enhance. Enrich.
MEE Cw Cdsr return [Cooling tower divert] preheating DM Water
LP Steam
MEEC
CRB
Deaerator
PHE
CW Ret-
DMW DM
Water
Enhance. Enrich.
Impact of Wide Seasonal Temperature range related to
LPS saving with heat in warm water return from Condensers
Coal Fired Boiler Chemical Recovery Boiler
DM Water Flow : 20 m3/h DM Water Flow : 50 m3/h
Season Winter Summer
Season Winter Summer
Time Day Night Day Night Time Day Night Day Night
DM DM
Water 20-24 16-20 29-32 26-29 Water 20-24 16-20 29-32 26-29
ᵒC ᵒC
Temp. Temp.
LPS TPH 0.45 0.6 0.3 0.4 LPS TPH 1.1 1.5 0.75 1.0
Saving- Saving
Deaer -Deaer
Temp. ᵒC 16-24 26-32 Temp. 16-24 26-32
range range
CER tCO2e
120 80 CER tCO2e
/month 200 300
/month
Enhance. Enrich.
With PHE installation, DM water Pump pressure had been
reduced with VFD from ………………………….: 12 ksc to 5 ksc.
Enhance. Enrich.
With PHE installation, DM water Pump pressure shall be
reduced with VFD from ……………………….: 12 ksc to 5 ksc.
Enhance. Enrich.
ENERGY GAINS & DECARBONIZATION
ASC +APC Reduction & Net Heat Rate Improvement
Enhance. Enrich.
NET ENERGY AVAILABLE & NOT GROSS ENERGY GENERATION
OTHERS
APC ASC
Centre Unit Reduction Scheme Centre Unit Reduction Scheme
Boiler BFP • High η [77% ]with Low DP Boiler Deaerator • Hot Process Condensate
CV return total &
• Hot Condensate Polishing
Boiler Fans • High η [> 80%]
with/without VFD Boiler SCAPH • Optimizn of Steam
pressures,
Boiler ESP • Energy efficient • Condensate air heating &
Transformers, • Effective Insulation
• Design & Optimization of
rapping Boiler Blow-down & • Minimization & Avoidance
Leaks
CPP Air Compressor • Waste heat[80%] to
Steam for Power gen. Boiler Soot-blowing • Optimization &
• HPS fm Blr to MPS from ST
STG CW Pump • Avoid CV throttling &
High η CWP STG Generator Air • CW to DM water &
[>86%]+Optimization Cooler • Turbine return condensate
Enhance. Enrich.
NHR –APC+ASC- Reduction Tips
Feed water temperature increase due to Pressure rise in BFP increasing steam
economy
Generator Air Cooling with Boiler make-up water & turbine condensate
CPP Air Compressor- Waste heat recovery -Boiler make-up water heating
Enhance. Enrich.
CONCLUSIONS & ADVISORY
INNOVATIVE ECS # 01 [ APC-Redn.]
With Cooling water flow lowered distribution in the 2 Condensers, through stoppage & running of 1
of 2 CW Pumps, significant APC reduction/Energy savings are being accrued on a sustained basis.
With this demonstration, stage is now set for varying the cooling water flow in line with varied turbine
exhaust steam condensing flow by going in for proposed Energy efficient smaller CWP with VFD
alongwith existing MCW Pump in place. With VFD in place, reduction in MCW Pump Power shall be
ensured at all condensing loads –high [35 to 50 TPH], medium [ 30 to 35 TPH & low [ 20 to 30 TPH].
Recommendation is one of varying Cooling water flow with condensation steam rate, CW conditions
[ ambient ], condenser exhaust steam state , so as to minimize ST exhaust steam enthalpy so as to
reduce NHR on a sustained basis.
Both of the above Innovative ECS contribute to reduction in NHR of CPP complex;
The schemes can be replicated in all CPP/TPP so as to achieve NHR reduction on a
continuous basis.
Enhance. Enrich.