Accepted Report VT-SUM
Accepted Report VT-SUM
GOVERNMENT OF INDIA
MINISTRY OF CIVIL AVIATION
AIRCRAFT ACCIDENT INVESTIGATION BUREAU
Foreword
This report has been prepared based upon the evidences collected
during the investigation, opinion obtained from the experts and laboratory
examination of engine. Consequently, the use of this report for any purpose
other than for the prevention of such future incidents could lead to
erroneous interpretations.
INDEX
CONTENTS PAGE No.
1 02
FACTUAL INFORMATION
1.1 HISTORY OF THE FLIGHT 02
1.2 INJURIES TO PERSONS 04
1.3 DAMAGE TO AIRCRAFT 04
1.4 OTHER DAMAGE 04
1.5 PERSONNEL INFORMATION 04
1.6 AIRCRAFT INFORMATION 07
1.7 METEOROLOGICAL INFORMATION 17
1.8 AIDS TO NAVIGATION 17
1.9 COMMUNICATIONS 17
1.10 AERODROME INFORMATION 18
1.11 FLIGHT RECORDERS 18
1.12 WRECKAGE AND IMPACT INFORMATION 19
1.13 MEDICAL AND PATHOLOGICAL INFORMATION 19
1.14 FIRE 19
1.15 SURVIVAL ASPECTS 19
1.16 TESTS AND RESEARCH 19
1.17 ORGANISATIONAL & MANAGEMENT INFORMATION 23
1.18 ADDITIONAL INFORMATION 23
1.19 USEFUL AND EFFECTIVE TECHNIQUES 27
2 ANALYSIS 27
2.1 GENERAL 27
2.2 SERVICE BULLETINS ON BEARING COMPARTMENTS 28
SEALS
1. Aircraft Bombardier
Nationality Indian
Registration VT-SUM
1
1. FACTUAL INFORMATION.
board the aircraft. On the day of incident prior to the incident flight,
Jabalpur. At 0830 UTC, while cruising at FL 250 and about 140 Nm from
Hyderabad cabin crew reported to PIC that there is smoke in cabin. The
PIC asked co-pilot to verify the smoke and the same was later confirmed
by him. The PIC instructed the cabin crew to check the cabin for any
source of fire. The cabin crew checked the whole cabin but did not find
any source of fire. The cockpit crew then decided to divert to Nagpur
which was around 80 Nm from their position. At around 0833 UTC, the
cockpit crew contacted Nagpur ATC and informed that they are making
priority landing at Nagpur due to smoke in cockpit. Crew also asked for
UTC full emergency was declared at Nagpur airport. The aircraft was
then cleared by ATC for landing at Nagpur with visibility 3200 meters
and winds calm. During descent, aft baggage cargo smoke warning along
2
with fire detected warning light came ON at master warning panel in
cockpit and the aft cargo fire extinguisher was operated from the
cockpit. Thereafter, the smoke was also felt in the cockpit and as per
the statement of PIC they have donned the oxygen mask. PIC then
for fuselage fire, smoke or fumes. The crew heard the aural warning
them to secure the cabin and informed that they are going to land at
Nagpur. During approach, low oil pressure warning for engine # 2 came
ON. At 0856 UTC, the aircraft landed safely on runway 32 and taxied
to the main isolation bay with follow me service and CFT’s. After
reaching bay, the PIC shut down the engine and instructed cabin crew to
evacuate passengers from the left side. All passengers were evacuated
from the left side. As per the statement of the cabin crew, post
evacuation while carrying out the cabin search they observed some
inflated life vests lying in the cabin. There was no injury to passengers
during evacuation. The crew also evacuated the aircraft from the left
side. At 0923 UTC, full emergency was withdrawn by ATC. There was no
On ground, engine oil level was checked, but nothing was visible in sight
glass. “Chip detector” message was found in “Eng health history”. Test
was carried out for chip detection wherein few metallic particles were
found which were out of limits. Engine was removed for further
3
1.2 Injuries to persons.
the engine was sent to OEM facility for investigation. The investigation
team participated in the strip examination and the details are covered in
Para 1.16.
Nil
AGE 27 Years
License ATPL
Category Aeroplane
4
Date of FRTOL issue & validity 22-Mar-15 valid upto 21-Mar-20
5
1.5.2 Co- Pilot:
AGE 28 Years
License CPL-11254
Category Aeroplane
6
Last flown on type 23-Nov-2017 (DHC 8 Q400)
The aircraft bearing MSN 4402 was manufactured in the year 2012 and
the maximum all up weight is 29,257 Kgs. At the time of incident, the
The aircraft was fitted with two PW150A engines. As on 24.11.2017, the
left Engine (PCE-FA0890) had logged 13063:41 hrs and 12640 cycles and
the right Engine (PCE-FA0807) had logged 11328:53 hrs and 10871 cycles.
The aircraft and its engines are maintained as per the Maintenance
7
The last major inspection was carried out at 11653:39 Airframe hours /
The aircraft was last weighed on 26.02.2017 and the weight schedule was
balance since last weighing. Prior to the incident flight, the weight and
The engine has a low pressure (first stage) axial compressor and a high
8
1.6.3 Bearings
There are nine main bearing on the engine: six roller bearings and three
ball bearings. The ball bearings No. 1, 3 & 4 withstand the following
thrusts:
Bearings number 2, 2.5, 5, 6, 6.5 and 7 are roller bearings. They support
radial loading and permit axial movement caused by thermal expansion. The
following table gives the direction of rotation of bearing along with the
Shaft Shaft
No. 7 Roller
9
The forward end of the HP (High Pressure) shaft is located longitudinally
The aft end of the shaft is held radially by a roller bearing (No 5),
combustor.
the HP spool.
Air entering at the engine inlet is directed rearward and compressed. Two
purposes. Air is first ducted to the low-pressure axial compressor and then
stage of compression. The compressed air then enters internal ducts, and
is discharged into the combustion chamber where fuel is added and ignited.
10
1.6.5 Bearing Compartments Sealing:
The No. 2 and 2.5 bearing cavity is sealed using 2 different types of
seals. The front end is sealed by a face carbon seal, the rear end is
sealed by a double carbon seal ring and the clearance left between the
a single carbon seal ring mounted in the LPC rotor. The 2 carbon seal
The No. 3 and 4 bearing cavity is sealed on each end using a double
carbon seal ring and the clearance left between the LP and the HP
shafts is sealed by 2 single element carbon seal ring. All seals are
The No. 5 bearing cavity is sealed on each end using a single carbon seal
The No. 6 and 6.5 bearing cavity is sealed on each end using a double
carbon seal ring and the clearance left between the LP shaft and the
The No. 7 bearing cavity is sealed on the front end using a double
carbon seal ring. The seal is pressurized with P2.5 (LP compressor
11
Brush Seals:
Wire type air restrictors, ensure proper air distribution between turbine
stages. Also ensure proper air distribution to cool HP turbine disk and
12
Bearing Cavities # 6, 6.5 & 7
1.6.2.4 PW150A CABIN BLEED SYSTEM
bleed air for the various aircraft systems including pneumatic system,
(HP/P3). As the two bleed ports are connected to the same duct, a
P2.7 check valve is installed in the low pressure port to prevent back
flow from the high pressure (P3) to the low pressure (P2.7)
In general, the ECS is supplied with low pressure air (P2.7). At low
13
supply allowing the P2.7 check valve to open and feed the airframe
Operation:
During low power setting, the bleed air is extracted from the high pressure
port P3 and during high power setting the bleed air is extracted from low
pressure port P2.7. The P2.7 check valve is installed on the inter-
14
compressor case in order to prevent back flow from high pressure bleed air
When power is reduced i.e. when P3 pressure is less than 77 PSIA, the P3
Shut-Off Valve opens allowing P3 port to feed the bleed air to ECS. The P3
air also flows back to P2.7 check valve and since its pressure is higher than
that of the P2.7, the two flappers on the P2.7 check valve are moved down
Shut off valve closes making P3 to stop feeding the bleed air to ECS.
Hence, the bleed air from P2.7 is the only pressure force applied on the
flappers causing the valve to open. The bleed air from P2.7 now takes over
15
1.6.4 CHECK FIRE DET warning light and Smoke Warning Light
CHECK FIRE DET warning light
When a fire overheat condition occurs, the alarm signals are processed by
the Control Amplifier then sent to the Fire Protection Panel in the flight
compartment.
If a fire or overheat condition occurs in either engine, this will cause the
gas within the APD to expand and turn ON the following lights in the
flight compartment:
fumes, the flight crew is required to land the aircraft without, delay
16
while completing fire suppression and / or smoke or fumes evacuation
procedures.
The following is the Met report of Nagpur Airport on the date of incident
1.9 Communication:
There was always two-way communication between the ATC and the aircraft.
At the time of incident, the aircraft was under the control of Nagpur ATC.
17
1.10 Aerodrome Information:
079° 02' 54" with elevation of 1033 feet. Aerodrome Rescue & Fire
The Cockpit Voice Recorder (CVR) and the Digital Flight Data Recorder
(DFDR) were downloaded and the information has been used for
investigation purposes.
The smoke warning remained till the engines were shut down after
landing.
warning came ON with master warning for 3 seconds. The Check Fire
Detect warning remained till the engines were shut down after landing.
18
At 084856 UTC at an altitude of 3086 feet, the right engine oil
At 085052 UTC, the right engine oil pressure warning came again and
remained till engine shut down after the aircraft was parked.
At 085530 UTC, the aircraft landed with flap 15, power lever left at
32.6, power lever right at 27.2, torque left of 0.5% and torque right of
4.5 %.
The master caution again came ON at 085729 UTC & 085810 UTC for
Both pilots had undergone preflight medical check prior to the first flight.
1.14 Fire:
The involved engine was removed from the aircraft after the incident for
detailed examination. The tear down inspection was carried out at OEM
designated overhaul facility. The relevant extract and findings made at the
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OEM designated overhaul facility during the teardown inspection are as
below.
Externally, there were no signs of oil leaking. The magnetic Chip Detectors
were found to have a little metal pickup. Some parts like the 2.2 and 2.7
Bleed off Valve (BOV) showed oil wetting on the internal passages. The 2.7
BOV (Blow–Off Valve) was wet on the external surface. Externally visible
oil lines were found to be satisfactory with no obvious leak areas. The Low
20
The o-rings of the RGB (Reduction
The oil screen at the Inter Compressor Case was found to have carbon like
After disassembly of the hot section, the area outside No. 7 bearing
compartment was found dry and the carbon seals were found in satisfactory
condition.
The oil staining was observed in the gas path indicating that the oil leak was
upstream. There was sooting or white discoloration throughout the gas path.
21
No. 1 Brg. – Flaking at cage No.2.5 Brg. Dents on
Roller Elements
22
Wave spring of No. 3 bearing carbon seal assembly had broken
The airline is a scheduled airline and were having a fleet of 35 Boeing 737s
permit (S-16) of the Airlines was valid till 30/06/2018. The Company is
to the CEO.
The airline has in-house maintenance facility and maintenance activities are
23
1.18.1 On 08.04.2018, during cruise, No. 2 engine of one of the other
from its intended flight due to pungent oil smell and smoke in cabin with
The smoke soon disappeared but the pungent smell continued without
the engine was replaced and investigation was carried out at OEM
given below.
The examination of the engine revealed oil wetness from P2.2, P2.7 and
P3 bleed ports. Internal inspection was carried out through P2.2 bleed
port after removal of the bleed valve. Presence of oil at the bottom of
the LPC case internal surface was observed. The high pressure turbine
(HPT), low pressure turbine (LPT) and power turbine (PT) could be
rotated freely. The main oil filter, the RGB scavenge filter were found
dirty/darkened and displayed some carbon debris. The main oil tank
The turbo machinery (T/M) magnetic chip detector (MCD) showed some
debris. The reduction gearbox (RGB) scavenge MCD and the RGB Air
conditioner generator MCD were however clean. T/M & RGB Oil samples
24
As per the report of OEM, the reported smoke in the cabin was caused
by the distressed No. 2.5 and No. 3 bearing carbon seals that resulted
in internal oil leakage into the compressor secondary air systems and
engine bleed air system. The carbon 2.5 seal was axially reduced of its
incident of smoke in the cabin and in the flight compartment. When the
flight was 20 nm away from Bangalore and at 10000 ft, a mild smoke
was observed along with smell in cabin. The non normal checklist actions
flight compartment, but the smell was still present. The Aircraft
out and all passengers and crew deplaned safely. The passengers were
taken to the terminal building. Post flight, no fire was observed in the
compartment.
The subject engine was removed and was stripped at OEM Centre.
25
External examination of the engine revealed oil wetness from the P2.2,
P2.7 and P3 bleed ports. Inspection through P2.2 bleed port after
the LPC case internal surface. The high pressure turbine (HPT), low
pressure turbine (LPT) and power turbine (PT) could be rotated freely.
The main oil filter and the RGB scavenge filter had carbon debris. T/M
and RGB Oil samples were dark, and the RGB samples also displayed
some debris.
As per the report of OEM, the presence of oil leakage at the P 2.2
valve in this case was confirmed. The reported smoke in the cabin was
caused by the distressed No. 2.5 and No. 3 bearing carbon seals that
The tension spring of no. 2.5 bearing carbon seal displayed fretting
(HSR) work scope, irrespective of any work scope that may be planned
26
1.18.3.2 Service Bulletin (SB) 35341
oxidation can occur on No. 3 bearing carbon seal while operating under
high temperatures and humid environments which can cause oil leakage
from No. 3 bearing carbon seal. To obviate the problem, SB No. 35341
was issued for all the PW150A engines on 6/10/2016 having S.No. PCE
– FA1238 or earlier.
As per this SB, the existing carbon seal was to be replaced with a new
one (as and when sub assembly is disassembled and access was
As the manufacturer has observed that the spring load range of no.
35342R1 was issued on 24/1/2018 which required that No. 2.5 bearing
seal be replaced with new one that has an increased minimum spring
load to prevent potential spinning of the air/oil bearing seal ring (as
NIL
2. ANALYSIS
2.1 General:
The aircraft was having valid Certificate of Airworthiness and Certificate
complied with. There was no snag reported prior to the incident flight.
27
Both pilots were appropriately qualified to operate the flight. The weather
was fine. The aircraft was always under positive control of ATC units.
The manufacturer had issued two service bulletins for PW150A engines for
No. 3 bearing carbon seal and No. 2.5 bearing seal. Both these SBs
required hardware replacement and was to be carried out as and when the
Service Bulletin 35341 replaces the #3 Brg. carbon seal with one made
humid environments. Similarly, the SB No. 35342R1 requires that No. 2.5
bearing seal be replaced with new one that has an increased minimum
spring load to prevent potential spinning of the air/oil bearing seal ring.
Scrutiny of the engine records revealed that though the engine had a shop
visit earlier, No. 3 bearing compartment Carbon Seal was of pre Service
during that shop visit was that the area of the engine required for
replacement could not be accessed which is in line with the SB No. 35341
In the present case, the #1, #2.5, #3 and #4 bearings had all suffered
Seal that had failed in service and caused oil to leak into the gas path. This
28
caused oil fumes to be released into the aircraft cabin through the Bleed
Off Valves. Eventually enough oil was lost to cause the engine to loose oil
pressure and trigger the Low Oil Pressure indication in the cockpit.
above due to oil smell by flight crew/ maintenance crew. The reason in both
these cases was No. 2.5 & 3 Bearing Carbon seal distress for which the
the existing carbon seals were to be replaced with new ones as and when
part.
The replacement was to be done during the shop visits subject to the
condition that access to the concerned area was available. As this could
have taken certain time, the operator has taken proactive measures in
aircraft.
carbon seal.
rental engines from its fleet before December 2018. These engines (pre
29
SB) are being monitored at repeat weekly oil sampling program with
In the meantime, the operator advised its flight crew and engineers about
the cabin smoke issue due to internal oil leak on the engines where the
3. CONCLUSIONS:
3.1 Findings:
a) The Certificate of Airworthiness, Certificate of Registration and the
incident.
complied with.
d) On the day of incident prior to the incident flight, the aircraft had
e) During the incident flight, while cruising at FL 250 and about 140 Nm
g) The cockpit crew then decided to divert to Nagpur which was around 80
Nm from their position and asked for priority landing due smoke in
cockpit. Crew also asked for emergency descent and safety services on
arrival.
h) During descent, aft baggage cargo smoke warning along with fire
30
the aft cargo fire extinguisher was operated from the cockpit.
i) The crew heard the aural warning (smoke detector) for lavatory and the
j) During approach low oil pressure warning for engine # 2 came ON.
k) During the tear down inspection at OEM facility, it was observed that
l) Failure of No.3 bearing carbon seal in flight caused oil leakage into the
gas path and oil fumes released into the aircraft cabin through the
Bleed Valves.
about the cabin smoke issue due to internal oil leak on the engines.
n) During the course of subject investigation, there were two more similar
occurrence reported. In both the cases the engine was removed due to
oil smell on ground by flight crew/ maintenance crew. The reason in both
these cases was No. 2.5 & 3 Bearing Carbon seal distress for which the
o) As per these SBs, the replacement was to be done during the shop visits
available. As this access to the area could have taken certain time, the
p) The operator intends to remove and return rental engines with un-
modified seals from its fleet before December 2018. Till that time, the
engines (pre SB) are being monitored at repeat weekly oil sampling
31
3.2 Probable cause of the incident
resulting in oil leak into the gas path causing oil fumes getting into the
4. SAFETY RECOMMENDATIONS
32