20170831focus Light
20170831focus Light
Name Position
Team Leader JM. Jeong QA Group , Manager
When:
Date of notification – 17,July, 2017
NO.2 Poor Surface
Was detected in which process:
Customer incoming Inspection
How much
Affected Lot # and Quantity :
Defect rate : around 52.25% NO.3 White Mark
Customer Information
Product Name
(Customer) Detected
Defect rate
Quantity
HCS Base Seat 151 52.25%
D3 Containment Actions
# Action Items
1 Check retain sample for the same/ similar defect mode, and than perform failure analysis before receive the
defect sample from Focus Light if there is any.
1.Re–inspection status : We have no stocks
2.We inspected the product that was shipped 11, August.
Result: We can’t find Mixing a part , bump and any defective part
Start & Due date : 11, August , 2017 Responsibility :S.Y. kim (QA.) Status/Result : Closed
1. Checked the process history , manufacturing , Final Test and KOSTECSYS 19~20 July,2017 detected abnormality
packing process
Start & Due date : 19~20-July. Responsibility : J.M, Jeong(QA) Status/Result : Closed
D3 Containment Actions
# Action Items
3 Material disposition for the parts at vendor site,
Start & Due date : 28- July ,2017 Responsibility : G.H.Lee (Prod.) Status/Result : Closed
4 Recovery plan to support Focus Light production.
Result:
- Detail delivery plan :
We will plan to delivery improved product by corrective action from next Shipping order.
Start & Due date : Unknown Responsibility : Paul. Park(Sales) Status/Result : Open
D4 Root Cause Analysis
Fishbone Analysis
Machine Material
Poor
Poor Cleaning
Cleaning Inspector
Inspector Mistake
Mistake
Method Man
D4 Root Cause Analysis
Fishbone Analysis
*.*. Fishbone
Fishbone factors
factors check
check result
result
Raw material For Raw material , there are not detect any abnormality Low
Material
Non woven fabric For Material for Packing we detect abnormality High
Unstable working
For the plating line, the unstable condition was not found Low
condition
Method
Regarding poor operation, there are detected any
Poor Cleaning High
abnormality.
1. Bump
■ Bump : We assume that the root cause is that mixing a part caused by Worker’s mistake
2. Poor Surface1
2.1) Picture Analysis(X20)
Spectrum1
Spectrum2
C :7.78%
C : 49.83%
Si : 10.31% Au : 89.12%
Au : 3.22%
Ca :0.97 %
2. EDAX Analysis result :
1) It is detected C, Si ,O ,Na ,Cl, Ca and Au in Spectrum 1 and is detected C, Ni ,Cu, Au to spectrum 2,
The Important thing is that it is Si content of spectrum 1(10.31%) much higher than it of Si of spectrum 2(0.00wt%).
2) Content of Ca of spectrum 1 (0.97wt%) more higher it of spectrum 2(0.00wt%)
Au plating seems to be serious damaged because it is affected by another material
D4 Root Cause Analysis
Defect Sample Analysis
3. Poor Surface2
3.1) Picture Analysis(X20)
Spectrum3
Spectrum4
Result : We can see black spots as a little bit of leaning product. When Product is in horizontal status
Black spot is colored
D4 Root Cause Analysis
Defect Sample Analysis
4. White Mark
4.1) Picture Analysis(X20)
Spectrum1
C : 8.95% C : 5.46%
Au : 83.22% 86.51%
2. Poor Surface
1) We assume that that poor surface 1, 2)poor surface 2 is caused by poor cleaning
method
■ Corrective Action
1. Bump: 1) Designating clear zone for good and defective part , waiting for inspection
Before
Before After
After
Micro Scope
Defective Product
Good product
Waiting zone
There
There ss nothing
nothing clear
clear zone
zone for
for good
good ,,
contents
contents defective
defective and
and waiting
waiting inspection
inspection
contents
contents Designating
Designating Clear
Clear zone
zone
2) Implemented training
contents) How to use each zone training report
■ Corrective Action
We changed the intensity of ultrasonic and cleaning time
Before
Before After
After
Ultra Intensity
Intensity of
of Ultrasonic :: 1ST contents Ultra Intensity of Ultrasonic : 4th Stage
contents
contents
ST Stage
Stage contents
sonic Cleaning
Cleaning time:
time: 10Min
10Min sonic Cleaning time: 15Min
D6 Verify Corrective/ Preventive Action
■ Corrective Action
3. White mark: Change the packaging material
Before After
contents
contents Non woven fabric contents
contents Clean
Clean Paper
Paper for
for clean
clean room
room
D6 Implement Corrective/ Preventive Action
1.WI is posted each facilities and worker keep the WI(Work instruction)
2. Product is inspected by inspection or Work instruction or mor
3. Change packaging material: We will plan to verify from next focus light order about
changing packaging material.
D7 Recurrence Prevention
Item Yes/No Evidence if Yes
Fan-out No N/A
FMEA No N/A
Before After
3.Revised FMEA
D8 Approval
Name Position
Report Provided by JM. Jeong QA Group, Manager